Folkston DERAILMENT Update

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  • Опубліковано 21 сер 2024
  • We now have new details about the April train collision in Folkston, Georgia.
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КОМЕНТАРІ • 133

  • @thomasmackowiak
    @thomasmackowiak 3 місяці тому +36

    Thank you for this information on the CSX incident in Folkston, Georgia in April! I am looking forward to any updates that you can give us in the future.

    • @QUIX4U
      @QUIX4U 3 місяці тому

      www.ntsb.gov/investigations/AccidentReports/Reports/RAR2003.pdf
      Will this do?

  • @jwslijm7278
    @jwslijm7278 3 місяці тому +22

    In the far distance this accident was captured on Virtual Railfan.

  • @DavidNewmanDr
    @DavidNewmanDr 3 місяці тому +21

    I hadn't heard of any derailment of a train in Folkestone, next to the Channel Tunnel entrance. Then I realised it's in Folkston.

  • @Motorman464
    @Motorman464 3 місяці тому +28

    There was a signal suspension, PTC was cut out and trains were running on block authority. The Restricted Speed rule was added AFTER this incident. At the time of the incident the crew simply had to contact the "switch tender", who is the conductor on the ground assigned the responsibility of lining and locking the switches for the movement of the trains coming through that location. The crew contacted the switch tender. He told they were lined up correctly.
    When a switch is removed from power to hand throw, sometimes the handle has to be thrown back and forth before it engages and allows you to actually move the switch points. The inexperienced conductor took it off power and put it in hand throw and threw the switch lever but did not ensure that the switch points changed direction. Maximum speed during this signal suspension was 40mph not including any other temporary speed restrictions, of course. The train came through and all the bad sh*t happened. The railroad is squarely to blame for this. First, in the past, we ALWAYS had a transportation supervisor present. ALWAYS. The switch tender screwed up but the lackadaisical culture is thick with the railroad. It started with Hunter and continues to this day. Their chickens have come home to roost.

    • @Sevenfeet0
      @Sevenfeet0 3 місяці тому +1

      So in other words, human error and possible poor process rules to prevent accidents like this from happening.

    • @allenra530
      @allenra530 3 місяці тому +5

      When I moved from MOW to environmental cleanup of a nuclear site, the training in human error and error precursors went from every 5 years to a yearly recertification in every aspect of error prevention. The world of railroading is just as dangerous as dealing with nuclear waste, but the safety emphasis is very different. I think that this is because railroading is so much older than the nuke industry and nuclear operations rules were developed mostly by the Nuclear Navy of Admiral Rickover. Civilian nuclear operations are nearly all run by Navy veterans or people from the Department of Energy who were trained by Navy veterans. The railroads need to run their safety training the same way. Industrial Safety Officers should be at least as common as Division Supervisors and Road Foremen of Engines.

    • @outdoorfrenzy
      @outdoorfrenzy 3 місяці тому +4

      @@allenra530the railroad doesn’t want to pay for safety before it happens. They’d rather pay for it after it happens. Somehow the bean counters have managed to tell the higher ups this will save them money.

    • @QUIX4U
      @QUIX4U 3 місяці тому +1

      If your assumption were to be correct, ONLY the one train would have been involved and thus would have simply "split" an incorrectly thrown/partially open switchblade, with just the ONE TRAIN involved.
      This had absolutely nothing to do with a switch, which WAS correctly aligned for turning out the East bound train.
      The 100% problem, was that the West bound (on his own) engineer, simply disregarded the stop/red signal and idled through hitting the side of the East bound (who was actually doing nothing wrong, as the Eastbound had right of possession of the turnout.
      The westboundSHOULD have been stopped AND REMAINED STATIONARY at the red. but, idled througfh, possibly with the engineer completely ignorant, out of his seat, doing something else, or catching 40 winks, had his eyes shut.
      He - is the only one who did NOT do what he was supposed to do.
      WAIT at the signal, without moving.

    • @QUIX4U
      @QUIX4U 3 місяці тому +1

      @@outdoorfrenzy The "railroad" can't fix stupid, any more than it can, if the ptc is switched out for shunting and NOT reactivated before moving off, along the main.
      IF THE PTC HAD BEEN REENGAGED, THE TRAIN WOULD HAVE AUOMATICALLY REMAINED AT THAT RED SIGNAL.
      SADLY ONLY THE "ON HIS OWN" WESTBOUND ENGINEER WAS AT FAULT.
      Not the engine, not the signals, not the switch and not the track.

  • @azrailfan2717
    @azrailfan2717 3 місяці тому +18

    Thanks for the update. Glad that none of the injuries were life threatening. My theory is (and I may be wrong) is either the switch Tender didn’t line the switch properly, or a miscommunication between the dispatcher and the crew. Or the train crew had a lack of situational awareness. We shall see.

    • @ThePaulv12
      @ThePaulv12 3 місяці тому +1

      My take from what's so far known is the crew were speeding. They were doing 13MPH faster than their own regulations require in this situation. The maximum speed allowed was 15MPH but they were doing 28MPH, so they couldn't stop in time for the misaligned points which the regs pre-empted may occur in this situation.
      However reading Motorman464 comment (below), it seems they were allowed to 40MPH and it wasn't their fault at all LOL.

    • @codybussard3813
      @codybussard3813 3 місяці тому +1

      You both are clueless. Quit spreading stuff that you have ZERO knowledge of. They were not speeding and it definitely wasn’t “lack of crew situation awareness”

    • @azrailfan2717
      @azrailfan2717 3 місяці тому +3

      @@codybussard3813 That’s why I said “my theories” and I may be incorrect. Don’t need to be snippy about it 😒

    • @TheNemosdaddy
      @TheNemosdaddy 3 місяці тому

      ​@@azrailfan2717Why do you foamers speculate on stuff you know nothing about?

    • @QUIX4U
      @QUIX4U 3 місяці тому

      My theory is this, the engineer of westboynd, left on jis own, decided to ease west, to be where the conductor would meet, before they arrived, but as he'd incorrectly NOT re-engaged drrive mode (PTC ON) simply set gis loco into "crawl at maybe 1 or 2 notches, then simply went to sleep, as you tend to do, on one's own (mo one looking) and so - boomph, didn't wake until the train collided with something and OH Sh&t - too late so blamed the PTC.

  • @jeromeinthehouse-l7e
    @jeromeinthehouse-l7e 3 місяці тому +13

    This could of been completely prevented. They had a inexperience conductor controlling the switch. The guy had less than one year of service. It should had been a MTO with him.

    • @DaMeng3000
      @DaMeng3000 7 днів тому

      He had more than a year bud.

  • @alanswafford9964
    @alanswafford9964 3 місяці тому +3

    You have an outstanding channel and I have learned a lot from your videos. I retired about four years ago and got into railfanning. I live in Decatur, Alabama and have both NS and CSX trains. Thank you.

  • @mrtjbiga1784
    @mrtjbiga1784 3 місяці тому +12

    thanks for the update , hope to see more

  • @AMRailfan11
    @AMRailfan11 3 місяці тому +1

    Great video as always, glad everyone was okay, and track warrants can get tricky sometimes, on the short line I work for we are dark territory so lots of track warrants

  • @davenitsch6094
    @davenitsch6094 3 місяці тому

    Thanks for the info, looking forward to hearing your updates!

  • @wideslammer
    @wideslammer 3 місяці тому +2

    Good information. Thanks for posting.

  • @fluxthelycanroc9603
    @fluxthelycanroc9603 3 місяці тому +4

    Track authoritys are also common in 171 territory or dark territory as its known. If you've been on the savannah side of macon its almost completely dark territory except for a few spots around savannah

  • @chuxproductions1090
    @chuxproductions1090 3 місяці тому

    Thank you for some possible insight into the circumstances surrounding this incident!

  • @jeffreygosselin7576
    @jeffreygosselin7576 3 місяці тому +1

    Big thumbs 👍 up on your report!

  • @WH_Railfan84
    @WH_Railfan84 3 місяці тому

    Thank you for the update on the train incident. Continued success on your channel!!!

  • @danielneeley5480
    @danielneeley5480 3 місяці тому +5

    Good job on your reporting sir, main stream media could learn something from you 😅

    • @KaiHenningsen
      @KaiHenningsen 3 місяці тому

      Mainstream media usually does not depend on experts or even interested amateurs in their reporting, and (thanks to how media are financed) are primarily interested in getting clicks rather than reporting. That's why people who are not dependent on these clicks for their main income (an important caveat) are often (not always, sadly) better than professional journalists at reporting facts on a topic they are interested in.
      With anyone directly or indirectly deriving their main income from the clicks, you unfortunately always have to be careful. There are still some good ones, but the temptation to go for clicks over facts is always there.

  • @JoeBlow-jj9uu
    @JoeBlow-jj9uu 3 місяці тому

    Thanks for the update V12❤

  • @ChainsawNW1218
    @ChainsawNW1218 3 місяці тому

    Definitely sounds like a signal problem, nice coverage!🛤🚂

  • @mikeingeorgia1
    @mikeingeorgia1 3 місяці тому +1

    What happens in practice most often is that during these signal suspensions the trains run using blocks. They usually will have Trainmasters or Road Foreman at the terminals having job briefings with any crews coming on duty that will be operating through the suspension area. They even produce track diagrams highlighting the suspension area and the names of the blocks. The switch tender and the crews very likely know each other too. It all sounds simple enough, but everyone is half asleep and in a hurry. It only takes one incorrect action on the part of anyone involved to have an accident.

    • @KaiHenningsen
      @KaiHenningsen 3 місяці тому

      That's why it's important to have several pairs of eyes on the critical parts. unfortunately, that costs money and is an easy target for the bean counters.

  • @user-yb9sr8pp9o
    @user-yb9sr8pp9o 3 місяці тому +2

    Thanks 👍

  • @user-mr3ct1dm9p
    @user-mr3ct1dm9p 3 місяці тому +3

    At least there were no serious injuries--- this time.

  • @TheQwaz
    @TheQwaz 3 місяці тому +1

    There maybe multiple people to point fingers at regarding what happened but, the biggest has to be the switch tender on duty. They may have been inexperienced but, how hard is it to throw the switch then step up and visually confirm that the switch was lined correctly? The northbound wasn't allowed to come through until he said it was clear. Would've only taken a few extra seconds to check and they didn't. Another example of common sense not be used. They may have been under a lot of pressure but, seems all the more reason to leave no room for doubt.

  • @natgass8102
    @natgass8102 3 місяці тому +3

    fortunately it doesn’t happen very often and I’m sure rules will be changed after this incident to try and insure that it doesn’t happen again

  • @dalemartens2962
    @dalemartens2962 3 місяці тому +2

    The entire railway from west to east is worn out!

  • @markydee48
    @markydee48 3 місяці тому

    This explains a lot. When it happened, I asked why PTC didn't prevent it. Now I know that it was suspended for maintenance. Also, I had stated that the inter.odal should not have been routed towards the Jesup sub. This explains it all. Glad the crews were ok

  • @Billblom
    @Billblom 3 місяці тому +2

    Reminds me of the fatal accident in SC while installing some of the PTC equipment. Amtrak was approaching an industrial area. Dispatch told the train crew working in the area to clear the main line, .. The conductor didn't line a switch properly, resulting in Amtrak having a horrible accident. Throw in the accident (also in SC) where the NS train went into a siding and wrecked causing a huge chlorine leak. Graniteville cost lives, a factory, and destroyed homes. (Chlorine is not nice to deal with..) All due to mis-aligned switches. And of course, the Amtrak wreck in Michigan, where they had been working on the signals in the Amtrak owned track where the person working on the equipment had bypassed the switch so that the signal showed GREEN, when it should have been Yellow or Red. Humans are always capable of causing issues, and I have a feeling that a conductor or dispatcher is going to find new employment as a result of the Mess in the Funnel... Sad. Very Sad.

    • @KaiHenningsen
      @KaiHenningsen 3 місяці тому +1

      _(Chlorine is not nice to deal with..)_ Understatement of the century.

  • @jaybo3303
    @jaybo3303 3 місяці тому +1

    Great video!

  • @albertcyphers1532
    @albertcyphers1532 3 місяці тому +6

    Gee what a surprise CSX didn't slow down for the speed restrictions. They seem to not slow down for anything

    • @ffjsb
      @ffjsb 3 місяці тому +2

      "CSX" didn't have to slow down, the ENGINEER did...

    • @albertcyphers1532
      @albertcyphers1532 3 місяці тому

      @@ffjsb I'm sure he was obeying orders

    • @Arby1965
      @Arby1965 3 місяці тому +1

      Dude, don't be a hole! The engineer, my friend of many years, was going 38 in a 40 restriction. The "NEW" restricted speed requirement came after this incident. Some of you foamers can be so clueless sometimes. We are not free to just speed thru restrictions like a trucker on the interstate.

    • @ffjsb
      @ffjsb 3 місяці тому

      @@albertcyphers1532 Standing orders was for 15 mph... He was WAY over that...

    • @Arby1965
      @Arby1965 3 місяці тому

      @@ffjsb Wrong! Get your facts straight. I work this sub but what do I know?

  • @ldog19077
    @ldog19077 3 місяці тому +2

    Would love to see the dashcam video on this one.

    • @AbelG8781
      @AbelG8781 3 місяці тому

      It's on IG

    • @wccl
      @wccl 3 місяці тому

      ​@@AbelG8781I tried finding it but nothing showing up. Not that experienced with ig tho.

  • @kennethtiller7916
    @kennethtiller7916 3 місяці тому +1

    Good info

  • @AtkinTheory
    @AtkinTheory 3 місяці тому

    Got to see the aftermath of that. Pretty wild

  • @jeffreysheridan5205
    @jeffreysheridan5205 3 місяці тому +2

    Old Hunter would say, not so precision, you're all fired.

  • @MohammedHasanRaheem
    @MohammedHasanRaheem 3 місяці тому

    Great Work

  • @doubleutubefan5
    @doubleutubefan5 3 місяці тому +1

    Honestly that's a good safety rule.

  • @user-hf1ce6gm7p
    @user-hf1ce6gm7p 3 місяці тому

    Y'all need to put a camera there cuz this happens again if you got a camera sitting there they can see there's something sitting there and wouldn't have another train smashing into it

  • @paulkoza8652
    @paulkoza8652 3 місяці тому

    So other than the signal system and PTC being suspended, and the track under control of the dispatcher, and the speed of the intermodal train, we really don't know that much.

  • @MrMark85044
    @MrMark85044 3 місяці тому +1

    was it really head on or did it hit the rear of the rock train?

  • @markhawkins5324
    @markhawkins5324 3 місяці тому

    Very good V12

  • @DairyNS
    @DairyNS 3 місяці тому +1

    @v12productions What is the best spot for railfanning at Inman yard because I’m going this summer

  • @stnicholas1224
    @stnicholas1224 3 місяці тому

    this happened 1/2 a mile away from the live cam i watch

  • @AroyalGibus
    @AroyalGibus 3 місяці тому

    i never knewl about this but now that i do i wana be invested in it

  • @aaronl_trains_and_planes
    @aaronl_trains_and_planes 3 місяці тому

    Why haven't they added GPS to trains and, at least on the mains, turnout alignment info? If all 18 wheelers have them, along with navigation telling them and everyone else where they are and what roads are closed. Why can't they adapt that to the rails? (besides them crying that it will cost too much)

  • @DavidNewmanDr
    @DavidNewmanDr 3 місяці тому +1

    In other countries, they close the whole line section while they are working on signals. They don't run trains without signals (except for radio controlled ETCS).

    • @KaiHenningsen
      @KaiHenningsen 3 місяці тому +2

      And if ETCS goes down, the train _stops._ Of course, then they might get movement orders via radio - but around here, those work very much like those new CSX rules. Also, I don't know how it's handled over there, but around here, such orders must always be in writing, that is, both sides must write down those orders (typically on a form that already has options and fields for all the relevant details).
      Also, when someone cut two cables that controlled pretty much all of the north of the country (which was clearly intentional - it turns out part of that information was public but was not supposed to be), what happened was that they _stopped all trains in the north of the country._ All of them. Until they could re-establish signaling. Incidentally, a railfan found that same document and reported on it on UA-cam - the railway phoned him and asked him to please take that down, so he did and created a new video that didn't show the parts of the PDF with the critical info. I think it took at least another day or two before the info finally vanished from the railway webserver - I think I saw the first video, went to Google, and had no trouble finding that same document.
      Railways are people. People make mistakes. Computers can help, but there are always edge cases.

    • @Ron-u1z
      @Ron-u1z 3 місяці тому +1

      No we dont. In the UK we have hand signal staff. But we employ enough people to do the job properly.

  • @emmylovesyu1
    @emmylovesyu1 3 місяці тому

    Did anybody else see the camera footage from the engine?

  • @Bikerguy5845
    @Bikerguy5845 3 місяці тому

    Sounds like someone might want to take a time out!!

  • @roberthuron9160
    @roberthuron9160 3 місяці тому

    Back in the day,a General Order,would have been issued,and the area involved would have flagmen,and torpedoes would have been used to alert engineers and conductors that they were in a work area! The uses of flares,also would have been used,as a backup to the system! Mayhaps,the reintroduction of Rule 99,on flagging might prevent these obvious blunders! The bean counters,in the long run,cause more money being spent,and create more problems in the long term! Safety is never the problem,it's the attitude of both MANAGEMENT,and the workers,manning the details! Bad management has destroyed more companies,countries,and cultures,without fail! Thank you 😇 😊!

  • @michaelalan1546
    @michaelalan1546 3 місяці тому

    Well done

  • @Neil-ru7kw
    @Neil-ru7kw 3 місяці тому +1

    Murphy's law

  • @johnsadventures6783
    @johnsadventures6783 3 місяці тому +1

    Human error is what it boils down to.

  • @JustinsRailfanning
    @JustinsRailfanning 3 місяці тому

    Will there be a dashcam video view ever released?

  • @billloffler8637
    @billloffler8637 3 місяці тому

    Two mistakes, switch tender misaligned the turnout and engineer running over speed to stop the train of sight of a problem (misalignment of a turnout).

    • @whiteknightcat
      @whiteknightcat 3 місяці тому

      A - so it might seem
      B - no, speed was acceptable for the conditions and the rules at that time

    • @thomasklimchuk441
      @thomasklimchuk441 3 місяці тому

      You forgot the conductor he is also to blame Train run under the direction of the conductor

    • @whiteknightcat
      @whiteknightcat 3 місяці тому

      @@thomasklimchuk441 Nope. Both the engineer and conductor receive the same instructions from the dispatcher. If their track warrant authorized them for a specific speed range in a certain location, then they had no reason to believe the warrant was in error if no special instructions were specified.

    • @billloffler8637
      @billloffler8637 3 місяці тому

      Speed was don’t exceed that if faster than being able to stop in half the distance you can see. In other words if you meet another train coming towards you both could stop in time to avoid a collision. They could have seen the misalignment of the turnout and stopped in time with no problem before rear ending the work train that the misaligned turnout set them into.

    • @whiteknightcat
      @whiteknightcat 3 місяці тому +1

      @@billloffler8637 Was under the impression the restricted speed requirement was implemented AFTER the incident. Re-watched the video - apparently the restriction requirement was in effect at the time. If that's the case, then the I032 crew is likely jobless now.

  • @user-vh1uc6in7b
    @user-vh1uc6in7b 3 місяці тому

    What Happened To the CSX train Locomotives?!

  • @k5elevencinc0
    @k5elevencinc0 3 місяці тому

    Are we gonna get that cab cam footage?

  • @railfanjeremiah8654
    @railfanjeremiah8654 3 місяці тому

    Nice

  • @Buckskin1290
    @Buckskin1290 3 місяці тому

    Oh wow…. So sad..

  • @bjjt-nu9dx
    @bjjt-nu9dx 3 місяці тому

    You never said what happened: what trains were on which tracks, was a turnout misaligned?

    • @whiteknightcat
      @whiteknightcat 3 місяці тому +1

      Train I032 was NB on the Nahunta Sub Track #1. Train L743 was SB and holding Nahunta Sub Track #1 north of the switch at "the Throat", as it's known locally. I032 was supposed to have been routed diverging onto Jesup Sub Track #2 but was instead routed down the normal orientation into the standing L743. There is footage on the Virtual Railfan channel showing I032 as it heads toward the collision, followed by the sound of the impact and smoke rising in the distance.

    • @eleanorhodges8204
      @eleanorhodges8204 3 місяці тому

      For the life of me, I still do not see this as a “HEAD ON” collision. I see the damaged locomotives of the intermodal train. I see damaged and mangled hopper cars of the work train. But - I do not see any locomotives of the work train. It just looks to me like the intermodal ran into the REAR end of the work train. Hence: not a Head On collision. Someone please correct me (provide evidence) if I am incorrect on this point. Thanks

    • @whiteknightcat
      @whiteknightcat 3 місяці тому

      @@eleanorhodges8204 It was indeed a head-on collision. The lead units on the northbound I032 were ET44AH's #3299 and #3469. They collided with the power for L743, AC44CW #245, AC4400CWM #7256, and ES40DC #5402, shoving those three units back into their own train and shredding the hoppers. Video footage from the Virtual Railfan camera near the fire station captured I032 as it headed for the collision, including the emergency brake activation, the sound of the impact, and the smoke and dust cloud rising from the collision location that was hidden by trees.
      In the still pictures shown in this video, I032's power is the two units on the right side of the screen. The three units beyond that were the L743's power, with #5402 derailed through the remains of a hopper car.

  • @venne515
    @venne515 3 місяці тому

    Wasn’t this like the same incident when Amtrak hit csx head on a few years ago?

  • @Jbeezy01
    @Jbeezy01 3 місяці тому

    WOW

  • @Jbeezy01
    @Jbeezy01 3 місяці тому

    Happy national train day

  • @tomp8871
    @tomp8871 3 місяці тому

    After reading all the comments, where lies the fault? Anyone

    • @davidpearson3304
      @davidpearson3304 3 місяці тому +2

      Don’t read the comments. Just wait for the official report on the cause.

    • @glennfoster2423
      @glennfoster2423 3 місяці тому

      ​@@davidpearson3304 Well said. Best practice is exercised by those who do not speculate about the cause before all the facts are known.

  • @craigsharp7168
    @craigsharp7168 3 місяці тому

    😮

  • @rGrajan45
    @rGrajan45 3 місяці тому

    Had this happened in India, Biden would have remarked against India and anthoni Blinken would have visited India, on security concern.

  • @AwesomeAngryBiker
    @AwesomeAngryBiker 3 місяці тому

    I think you should prioritise the crew as very first fact, glad they're physically OK

  • @craigsharp7168
    @craigsharp7168 3 місяці тому

    😢😮

  • @tonyphillips1917
    @tonyphillips1917 3 місяці тому

    They should of shut it down until the problems was fixed csx money hungry

  • @szabados1980
    @szabados1980 3 місяці тому

    Wooden sleepers, nails and no electrification. Which skint third-world country is that?

  • @rudolffabrie3233
    @rudolffabrie3233 3 місяці тому +3

    One derailment after the other.

    • @jamesyoung7655
      @jamesyoung7655 3 місяці тому +1

      Derailments happen all the time just like car wrecks…. Just hearing more about them cause the media is getting a ton of likes and views

    • @KaiHenningsen
      @KaiHenningsen 3 місяці тому

      @@jamesyoung7655 Derailments in the US happen far too often. I looked it up a while ago, and if I remember correctly, it was something like one a day. Most don't make the news.

    • @jamesyoung7655
      @jamesyoung7655 3 місяці тому +2

      @@KaiHenningsen that’s because the US have way more trains running than any other country

    • @KaiHenningsen
      @KaiHenningsen 3 місяці тому +1

      @@jamesyoung7655 Not that much more. I wish I remembered more details - I think I contrasted it with numbers for either Europe or the EU, but I'm not certain. It's been a while.
      I'd say it's probably a combination of high traffic and the cheapest possible track maintenance. (And of course a few other things, but I think these two are the most important.)

  • @KimiWallrus
    @KimiWallrus 3 місяці тому

    Russian Solar Flare?

  • @dustup2249
    @dustup2249 3 місяці тому

    They are obviously doing it wrong.

  • @railfaninacar
    @railfaninacar 3 місяці тому

    Yooo

  • @thebops4180
    @thebops4180 3 місяці тому

    NOT GOOD ENOUGH! These type accidents are TOO common! Locomotives derailed hitting an empty a couple days back in a siding (live footage). Again WTF?

  • @how_to_hallagon1
    @how_to_hallagon1 3 місяці тому +1

    Maybe Joe needs to run trains so federal government will finally prosecute him. Seems to be easier that way

    • @paulholmes672
      @paulholmes672 3 місяці тому

      Nah, he'll have Pot Hole Pete in charge, working as efficiently as he has been in the past.

  • @ASILLYTRAINBOY2011
    @ASILLYTRAINBOY2011 3 місяці тому +1

    First

  • @SCLModeler
    @SCLModeler 3 місяці тому

    So much false information in this video, it’s pathetic and complete BS. Just say you don’t know what ACTUALLY happened and move on. You’re another reason why RR don’t like most Railfans 🙄

  • @Ron-u1z
    @Ron-u1z 3 місяці тому

    So they are blaming the crew. NOTHING to do with all the cutbacks with safety staff being fired in their thousands. Also the infrastructure in the USA is pathetic. Nearly every day their are derailments. It's a very rare thing to happen here in the UK or Europe.