Worst locked up engine ever!! With Mustie1!! Will It Run?

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  • Опубліковано 7 січ 2023
  • Mustie1 and I tear down this 1966 Ford falcons engine and Find a big surprise! Worst engine both mustie1 and I have ever seen. Will it run??
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КОМЕНТАРІ • 418

  • @braxtonnelson7422
    @braxtonnelson7422 Рік тому +40

    You know you're "Wrenchin' With Mustie" when your tool kit includes a fencepost and a sledgehammer! I'm a little proud of myself for finding where he was spending his time, and that it was well-spent helping a friend!

  • @TheMrShinagami
    @TheMrShinagami Рік тому +47

    I think the film you guys were referring to is Flight of the phoenix. made in 1965 with James Stewart. It was remade in the early 2000's but I've not seen that version.

    • @Oh-Jay52
      @Oh-Jay52 Рік тому +4

      Good Film !

    • @driveanalog747
      @driveanalog747  Рік тому +4

      You're correct! Now I need to watch it again!! Thanks for watching

    • @peregrine1970
      @peregrine1970 Рік тому +3

      Yep... original was good... the remake, not so much.

    • @TheMrShinagami
      @TheMrShinagami Рік тому +2

      @@peregrine1970 Isn't that always the way (with a very few exceptions).

    • @TOM2RN
      @TOM2RN Рік тому +2

      You are correct about the movie. It had Dennis Quaid and Hugh Laurie (House) in it. Remake was in 2004. Not a bad remake.

  • @baggins1
    @baggins1 Рік тому +30

    Flight of the Phoenix

    • @driveanalog747
      @driveanalog747  Рік тому +4

      Yes that’s the one!! Thank you!

    • @mrfishbulb7187
      @mrfishbulb7187 Рік тому +2

      Good film.

    • @tinybrown6710
      @tinybrown6710 Рік тому +2

      They crashed in the desert and a model designer came up with the phoenix from parts of the aircraft 😁

    • @baggins1
      @baggins1 Рік тому +1

      @@tinybrown6710 correct

    • @gregphillips.1312
      @gregphillips.1312 Рік тому

      Both the Original and the remake are great Films.

  • @kensherwood4866
    @kensherwood4866 Рік тому +29

    As a regular "Mustieite" I missed his usual weekend posting this week. When this popped up, bingo, I'm in. Love the rapport between you two and the banter adds to the fun. One things for sure Mustie1 never quits so stuck or not he was not going to be beaten. Thanks for posting

  • @smarthome2660
    @smarthome2660 Рік тому +6

    I was surprised to see you didn't remove the starter before removing the head. I bought a 1979 Mercury Zephyr with a 2.3L engine for $50.00 that I was told the engine was seized. I removed the starter and the Bendix was stuck into the flywheel. I installed shims on the starter and the car was in perfect condition.

    • @TiborRoussou
      @TiborRoussou Рік тому +3

      Yeah, I thinking it's not the Bendix that is stuck!

  • @joshjablonicky171
    @joshjablonicky171 Рік тому +11

    Been waiting for another video from you. Absolutely love your channel. First time ever seen you on UA-cam was with your buddy musty you two working together is hilarious always a lot of fun entertaining and you get whatever you two are working on going. As always thanks for all the hard work you put in the videos for us it is greatly appreciated

    • @driveanalog747
      @driveanalog747  Рік тому +3

      Ya it’s been a while. Life has been very busy. Things have slowed down a bit so I should be able to do at least one a week. Thanks so much for your support. Happy New Year!

  • @chatrkat
    @chatrkat Рік тому +6

    It’s fun watching two smart guys team up on a challenging project. The Falcon shall live again! Just not in this video. 😢

    • @MrPaige222
      @MrPaige222 Рік тому +1

      And not with that powerplant. She DONE

  • @RANDALLOLOGY
    @RANDALLOLOGY Рік тому +9

    I had a similar situation in a old cars valve train of goop built up all over and in-between the rockers. Later found out there previous owner only used Quaker State oil and didn't change it when required. The build up was paraffin. Thats what Quaker State used to put in their oil.

    • @rupe53
      @rupe53 Рік тому +2

      Quaker State was always great if you kept up on oil changes. Been using it since about 1970. It was one of the few low Sulphur oils back in the day.

  • @arnoldwinkelman1027
    @arnoldwinkelman1027 Рік тому +3

    Great vid! I know the feeling of being 'elbow deep' inside an engine one never should have touched... good luck with that project!

  • @thedevilinthecircuit1414
    @thedevilinthecircuit1414 Рік тому +2

    I'm the guy that drove that car into Frazer's Pond 45 years ago. I would've torn the engine down to get the water out of it, but sitting in jail for 90 days put the kibosh on *that* plan.
    A good backstory adds to the drama 😎

  • @skswig1
    @skswig1 Рік тому +8

    I love the old straight six's. The heads come off easier than changing the oil in some modern cars.

    • @Cartier_specialist
      @Cartier_specialist Рік тому +1

      From the looks of the inside of that engine I'm not sure the oil was ever changed.

  • @paulmartin8212
    @paulmartin8212 Рік тому

    I'm glad YT suggested this for me. I remember you from that flooded out Porche and maybe some other Mustie stuff. Glad you posted this. Man that was bad. Great old car and should be relatively easy to make it a driver again.

  • @gregphillips.1312
    @gregphillips.1312 Рік тому

    Being from the UK Mustie1 updates come in just before Sunday Lunchtime. I like to clean up the Shop in the morning and wait until I have settled down with a Beer early afternoon to enjoy his Episodes. Great to see him appearing in other UA-cam Creators Uploads! 🙏

  • @additudeobx
    @additudeobx Рік тому +1

    This reminds me of my first car. A 1963 Ford Falcon Sprint, with an over cammed 260 V8, a Holly 500 2bbl, a 4 speed Warner T-10 tranny with Hurst Shifter. I loved that car. I bought it in about 1970 and had it for about 15 years, had a family, had to sell it.
    My Mom had a brand new 1960 Ford Falcon Wagon with a 144 in-line 6. That car ended up with over 120K before the engine was rebuilt. She swore by Alimite brand oil.

  • @pks41805
    @pks41805 Рік тому +1

    I am so glad you're back.

  • @edkennard72
    @edkennard72 Рік тому

    What a great video thank you for posting it and it's good to see musty working with other people and the two of you together reminds me of Laurel and Hardy

  • @derekanderson4940
    @derekanderson4940 Рік тому

    good to see you back on tube awesome👍

  • @oculusangelicus8978
    @oculusangelicus8978 Рік тому +2

    Well done guys! I think that the Farmer who put it in the Garage decided to put extra coolant in the rad, but the head gasket was leaking and he kept putting water and coolant in it because he couldn't see the leak and ended up filling the block with water/coolant and then over the decades that it was sitting the coolant/water leaked out through the oil leaks that FORD always seems to have. Plus you also have to consider that the Falcon was a cheap car from the FORD line anyways so it was likely already predisposed to failure at some point, but the possibility of a filling of water inside the block would have rusted the engine components into one amalgous piece of solid rust. I have never seen a maintained engine look so badly in my life, and that is saying something.

  • @MrButtonpresser
    @MrButtonpresser Рік тому

    Great video guys. Great to see Mustie1 moonlighting.

  • @MrWalleye
    @MrWalleye Рік тому

    I'm liking the collaboration videos the guys are putting up these days compared to the solo talking to yourself ones. LOL

  • @Eremon1
    @Eremon1 Рік тому +2

    I watched a video of some guys that pulled a speed boat out of lake mead that had been under water since the 80's/90's and they got the engine to run some what. But that engine there looks like it was a boat anchor for several decades. Gotta wonder what happened.

  • @MaxNafeHorsemanship
    @MaxNafeHorsemanship Рік тому

    I daily drive a 66 Falcon that is in about the same shape. Love that car. That little 200 is so easy to work on too.surprisingly, parts are easy to get and cheap. Many Ford cars used the same parts.

  • @davecooper5951
    @davecooper5951 5 днів тому

    You're having a smashing time there ! Movie was "Flight of the Phoenix" - well worth watching for DIY nuts......

  • @kellykonoske91
    @kellykonoske91 Рік тому

    You say Mustie1 and Im there. Good to see you two working on something together.

  • @FastEddy5
    @FastEddy5 11 місяців тому +1

    Big mustie1 fan here! Subbed just because you are friends! Good stuff

  • @rust_hunter7867
    @rust_hunter7867 Рік тому

    Not nearly as badly locked up as that Marine Engine;) love your videos!

  • @larry3064
    @larry3064 Рік тому +3

    I've worked on a bunch of six bangers like that and I've never seen one that nasty. WOW

  • @ronaldclark2624
    @ronaldclark2624 Рік тому

    Thanks! Dollar wise it's a bust, But it could be a runner if repaired! So, here in video land, it should be about can do and not about the dollar, Heh? Love to see complete restorations even if they aren't mechanically perfect but usable. Ron🙂

  • @billdyke9745
    @billdyke9745 Рік тому +6

    Good to see you back. No shortage of discarded straight sixes out there in decent working order... 🇬🇧👍

    • @driveanalog747
      @driveanalog747  Рік тому

      I have a plan for this..It is a straight 6 but not a ford. stay tuned. Thanks for watching.

    • @johnalees99
      @johnalees99 Рік тому

      @@driveanalog747 Barra swap!

  • @PierreClavie
    @PierreClavie Рік тому

    Enjoyed the video, watched Mustie 1 for years!
    Cheers

  • @terryharris9741
    @terryharris9741 Рік тому

    I had a 1970 Ford Falcon Station Wagon, looked identical, 200 6 cyl eng. great car !

  • @timothynewkirk2654
    @timothynewkirk2654 Рік тому

    Jimmy Stewart - - - The Flight of the Phoenix, GREAT MOVIE. BTW Good Luck Guys! ...Newk from Kentucky

  • @davidstradtman8232
    @davidstradtman8232 Рік тому +1

    I have some wonderful memories from the back of a Ford Falcon wagon just like that one.

    • @MisterMikeTexas
      @MisterMikeTexas Рік тому

      Those were rare, weren't they? I don't recall seeing many mid to late 60s Falcon wagons.

    • @tomperry1048
      @tomperry1048 Рік тому

      wink, wink

  • @williamtanner1372
    @williamtanner1372 Рік тому +2

    Great to see a new video! That engine is trash but fun to watch the tear down.

  • @Fatterpilot
    @Fatterpilot Рік тому +5

    My guess is the owner never changed the oil. Detergent oils from the ‘70s were terrible at collecting carbon if you didn’t change frequently. I’ve seen heads caked worse than this one, and the engine was brought back to life. Good luck on the resto!

    • @driveanalog747
      @driveanalog747  Рік тому +1

      I think oil would have helped but it’s was pure rust inside! Nothing like I ever seen before. Thanks for watching

    • @jaykellett2327
      @jaykellett2327 Рік тому +1

      Someone sabotage the engine by pouring a quart of oil in it maybe? Or blown head gasket that leaked engine coolant into the oil somehow?

  • @robertweldon7909
    @robertweldon7909 Рік тому

    1/24/23
    This video reminds me of the first engine I helped tear down and get to run, a 1956 Chevy 265, in 1963 or 1964. We took it apart in the car. it was gummed up just about as bad. None of us knew what we were doing, but we got the old thing to run. This engine is junk, but it must have been fun digging into it. ;-)

  • @Batti2323
    @Batti2323 Рік тому

    That is the worst one I have ever seen! Thanks for tearing it down so we could all see this.

  • @orangepickel2
    @orangepickel2 Рік тому

    My parents bought the only 4 door Falcon wagon 3 to tree 170 cid 6. Fire engine red. Kept it driving 27 years before original clutch failed burned a quart of oil Every 500 miles 240,000 miles, $27.00 paid to junk yard to tow away. Island of Guam.U.SA. Teflon bushings in steering no grease fittings no power steering hard over to hard over with one finger when moving.

  • @Nine_Finger_Wrenching
    @Nine_Finger_Wrenching Рік тому

    How awesome was that to get to work with Mustie1?!? Super cool! Too bad about the old motor.

  • @johnminor2496
    @johnminor2496 Рік тому

    The movie was Flight of The Phoenix with Jimmy Stewart in 1965. Also, a remake in 2004 with Dennis Quaid.Fine video. Thank you.

  • @eskieman3948
    @eskieman3948 Рік тому

    Looks like a Ford 200ci six w/Autolite 1 barrel carb. They're OK as an engine, nothing great, I had a few Mavericks with them. I helped a friend free up a locked Chevy 235ci in a Chevy II by pulling the plugs, spraying Kroil penetrating oil into the cylinders, replaced the plugs & let it sit until the next weekend. Got it loose by both of us using a long breaker bar & just rocking back 'n forth many, many times.... we were fortunate compared to what you had to do with this puppy!

  • @hcox1111
    @hcox1111 Рік тому

    My first car was a 1968 Ford Falcon Futura 2 door with bucket seats and three on the tree. 200 6 cylinder engine.

  • @shrek_428
    @shrek_428 Рік тому +1

    Perfect candidate for a 390 or 428 FE, and starting in 66, it will fit, use Fairlane parts. Make one hell of a sleeper.

  • @kellykonoske91
    @kellykonoske91 Рік тому

    I think thats called "never having an oil change in its life"! Jeeeeze! Todd the retired trucker.

  • @fastacker2
    @fastacker2 Рік тому

    I learned to drive on a '67 Falcon (not a station wagon). 200 inline 6. My advise is to pay a junk yard to take it away. Pay him anything he wants! :)

  • @balsachopper7
    @balsachopper7 Рік тому

    Those pushrods looked the same as when l pulled the valve cover on my Ford p/u after using Quaker State oil for a year. Rocker arms were one big mass of goo. Pulled everything off the head and spent the day cleaning up everything. Put everything back together, drained the oil, added new oil plus quart of diesel fuel. Let it idle about 5 minutes. Repeated 3 times before the flushing came out clean. Will never use Quaker State again.

  • @watsisbuttndo829
    @watsisbuttndo829 Рік тому +2

    If that rig was in Australia it would be junkyard barra for the win!

  • @kenscott7825
    @kenscott7825 Рік тому

    My father had the same engine in his 63 biscayne. The valve cover was leaking and we went to replace the casket. When we pulled it off the is was filled with sludge. We used rags to remove as much sludge as we could. Great engine it ran for years with no problems.

    • @MrPaige222
      @MrPaige222 Рік тому

      Biscayne is chevy. This is a Ford.

    • @proofbox
      @proofbox Рік тому

      The Biscayne would have had a 230 CID which was new in 1962 as a 190 CID for the then new Chevy 2 compact and replaced the 235 engine used since 1936 in the full size cars a 230 or optional 250 were used and were far better than the old design and were used until 1986 until being replaced by the 4.3 V-6 and were still far better than the lumpy 4.3 which would knock your fillings loose with its constant vibration , it was used until the mid 2000's and even then it was still a rough running engine . [ and its gasket not casket on top of the motor ]

  • @leonhart2452
    @leonhart2452 Рік тому +1

    Check out fab rats yellow submarine series. A boat sank 30+ years ago. No rust inside. Turned over. Pulled heads and oil pan to check it out. Things looked great. Reassembled and it ran.

  • @charleshemsley4149
    @charleshemsley4149 Рік тому

    The movie was called flight of the fenix, Thanks for a great video.

  • @eskieman3948
    @eskieman3948 Рік тому +2

    Folks - what happened at 13:45? Video got switched around to a mirror image of the engine bay - carb & cylinder head went from left to right, goes back to normal at 14:27!

  • @Couch_PotatoMoJo
    @Couch_PotatoMoJo Рік тому +1

    It'd been great if I could have seen the engine bay. The light needed to be pointed at the engine bay, not the standing cam.

  • @proofbox
    @proofbox Рік тому +4

    This series of engines introduced in 1960 came in 144 , 170 . 200 and 250 CID through the mid 80'S . After that a 4 Cyl version was used in Tempos for a while , the number 3 main bearing is also the thrust bearing and a bit of a weak point . 260 and 289 V8'S were also used in Falcons . These are common engines and easy to find and usually use the Ford-O Matic which is a two speed unit . After 1970 302 with 3 speed autos were used in Mavericks and Mustangs You have lots of choices .

    • @marzsit9833
      @marzsit9833 Рік тому +1

      from the factory 144's were black, 170's were red, 200's and 250's were blue but the 250 block is one inch taller and the water pump has 5 bolts instead of four. the four cylinder version was used in tempo/topaz and some taurus/sables.

    • @MrGazzaj
      @MrGazzaj Рік тому +1

      @@marzsit9833 In Australia we had 221's as well

    • @tomtom3889
      @tomtom3889 Рік тому +1

      I have a 250 out of a mavic in my 1965 falcon

  • @eddiekilby
    @eddiekilby Рік тому +1

    I thought the 170 was the most common. My dad had a 66 mustang sprint 200. I remember getting parts from the junkyard from ford falcons basically the same car.

  • @stephenbonesteel664
    @stephenbonesteel664 Рік тому

    Have seen this before. Oil caked dirt on bell housing says it all . Bad rocker cover leak /pos rear main/ pos burning also= no change ,just add. Old dart slant 6 he even used drain oil he got for free. That one spun a cam bearing. Since the body was descent he parked it thinking he would get a wreck with good engine and swap . Never did, found this one garage of abandoned farm house . Found worn out slant irrigation pump engine in an estate sale in back of tractor shed. Over 30 years and more sludge turns to that stuff.

  • @ericchazankin4919
    @ericchazankin4919 Рік тому +1

    Looks familiar - my first car was a 1967 Falcon wagon; but that had a 289 V8, a vastly superior engine. Mine had a three speed automatic on the column. Mind you, I had lots of frustrating problems with the carburetor and automatic choke system - but when it decided to start, there was no shortage of power! And so much room in the engine compartment - could almost fit two motors in there.

    • @davidlockwood5946
      @davidlockwood5946 Рік тому +1

      I had a 68 Falcon two door with the same engine and transmission. I loved that car, it could fly!

  • @farnthboy
    @farnthboy Рік тому

    Must say what spicked my interest when l saw the thumbnail on this l thought it was an Aussie XT series Falcon released here in 1967. Looks identical to the Aussie Falcon exept the rear quarters & tail lights. The rear section looks likes its off a Fairlane & is longer than the XT series manufactured here. Engines here were the 200, 221 & 302 V8. Got an XW 1970 Falcon myself with the trusty 351cleveland - great aussie cars.

    • @nevillegoddard4966
      @nevillegoddard4966 Рік тому

      @farnthboy yeah I was gonna say it looks the same as an Aussie XR or XT falcon! Cool!
      Shame youse couldn't get it going but this donk is definitely falcon jammed up!

  • @xray111xxx
    @xray111xxx Рік тому

    Mustie1! Darren for real is the man making motors work!

  • @Dazzy84
    @Dazzy84 Рік тому

    "Hey guys, hows it goin' "
    If ya know, you know. Lol

  • @stevencox75
    @stevencox75 Рік тому +2

    Mustie1 is my favorite youtuber hands down

    • @driveanalog747
      @driveanalog747  Рік тому +2

      I hope I'm Your second favorite! Haha Thanks for watching.

  • @andyhamilton8940
    @andyhamilton8940 Рік тому +1

    Little Johnny put some Morton’s oil treatment in there for Gwampa

  • @markae0
    @markae0 Рік тому

    Some brake clean and it would be fine! LOL. Nice video of a tear-down.

  • @p52893
    @p52893 Рік тому +2

    I take all those old bolts out by hand, doing so makes one understand more problems that could be ahead.

  • @donaldshimkus539
    @donaldshimkus539 27 днів тому

    I know I'm a year late, but just found this video. Pull the 6 and slush box and you have room for a nice Coyote and T-6. YEAH BABY!

  • @jamesschaffner4916
    @jamesschaffner4916 Рік тому

    If I were to take a quick guess, I would suggest that the head gasket failed and pumped coolant through the oil system and that's what caused the engine to seize...These engines were known for bad head gaskets...

  • @Ragnar8504
    @Ragnar8504 Рік тому

    Ask Handtool Rescue if you can dunk the whole engine into his barrel of Evaporust 😀

  • @joostderidder
    @joostderidder Рік тому

    Engine is, indeed, in a pretty bad shape.
    I suppose that the car had an accident ending in a ditch/pool but without damaging the body. Or flooded, maybe? By the time, it wasn't worth the repair and it "ended" somewhere.
    Is this block repairable? Maybe. It would need a total dismounting ... honing etc etc ...
    Is it worth all the work as I suppose that those 6 cyl are still to find cheapo in the USA??? No. It isn't.
    Thanks for this vid! And happy 2023! (to you and Mustie).

    • @driveanalog747
      @driveanalog747  Рік тому +3

      Ya don't think its worth the time to rebuild but its and idea. I have a big surprise for an engine.Stay tuned. Thanks for watching!! Happy New Year!

  • @armaturespin
    @armaturespin Рік тому

    "Flight Of The Phoenix" with Jimmy Stewart is the movie you were think of.

  • @williamnichols429
    @williamnichols429 Рік тому

    Over the years I've seen more than one old ford six die because the oil pump drive shaft snapped. It only takes a minute to pull the distributor to check it.

  • @pratt1bp
    @pratt1bp Рік тому +1

    Don’t throw that block away. We got guys down here in Australia that chase those

  • @tonywall8991
    @tonywall8991 Рік тому

    OMG Mustie gave up. Never thought I'd ever see that. Lol

  • @flhusa1
    @flhusa1 Рік тому

    Put a breaker bar back on and put a little tension on it either direction and use a BFH to hit the breaker bar just below the head. Repeat both ways till it moves slightly and then just use Armstrong to finish. Been there done that got the scars on me and my tools to prove it. Never met a stuck engine I had to disassemble. One little flake of rust can hold it. Just need to jar it loose. Pulling on breaker bar will you nowhere.

  • @usernamesreprise4068
    @usernamesreprise4068 Рік тому

    The film was called flight of the phoenix, 1965 and starred Richard Attenborough and James Stewart among others

  • @manytrickpony695
    @manytrickpony695 Рік тому

    The mustie1 hammer. The mustie1 soldering iron. Is a favorite for me... admittedly I haven't seen it for a while it was huge!

  • @bmortlock1956
    @bmortlock1956 5 місяців тому

    A 50/50 mix of Acetone & ATF works wonders in cylinders & stuck rings.

  • @garysenecal7683
    @garysenecal7683 Рік тому

    Definitely call it ! To bad thought! When properly maintained its a bullet proof engine . Good job! There was no way that engine was running. Nice Falcon. Dont give up on it ! IT could be a yesterdays masterpiece today . It could be used to service another family for the next 125000 miles. Cool car guys !

  • @heathfiedler
    @heathfiedler Рік тому

    today on mustie1, we drop out the old locked up powerplant in a ford falcon and drop a in a v8!

  • @kman-mi7su
    @kman-mi7su Рік тому

    Wow amazing it was in a barn and filled with water like that. I'm guessing it was parked with a stuck open valve likely.

  • @redknight1322
    @redknight1322 Рік тому

    1965's Flight of the Phoenix, starring Jimmy Stewart, is the movie reference you're looking for. 👍

  • @illdoyouhere
    @illdoyouhere Рік тому

    if even mustie can't get it going, it will never go.

  • @michaelhill2844
    @michaelhill2844 Рік тому

    "Flight of the Phoenix" is the movie you're thinking of.

  • @jamesatkinson6480
    @jamesatkinson6480 Рік тому

    In Australia, about 2 to 3 years later ('68 to '69) Ford introduced an 'XT' model Falcon with a choice of 6 cylinder engines; 188 cu. in., and 221 cu. in. (3.6 litres) with identical looking grille and body pressings (station wagon). I wonder of the size of the 'locked up' engine. I understand there was a 300 cu. in. fitted to a base model F100, but don't know if fitted to this car?

    • @proofbox
      @proofbox Рік тому

      The Ford 240/300 six was designated for full size cars and trucks and was in production until 1997 , after being introduced in 1965 . It was only used in full size models for its entire life . And in terms of power and toque was considered the best American inline 6 ever made .

  • @victor58010
    @victor58010 Рік тому

    Please ,please drop the intrusive music! The conversation and the sounds of the tools is all the music we need.

  • @davidredfearn664
    @davidredfearn664 Рік тому

    Do I detect the absence of those pesky angle braces like in my 64 falcon?

  • @shinobiscience3299
    @shinobiscience3299 Рік тому

    "I make my livin' on the evening news!" 🎸🎸🎸

  • @larry3064
    @larry3064 5 місяців тому

    Them six bangers was bad about hanging up starters on the flywheel.

  • @terryrobinson1416
    @terryrobinson1416 Рік тому

    Mustie goes on vacation.... to another guys garage to help him work on junk... he is amazing!

    • @driveanalog747
      @driveanalog747  Рік тому +2

      He is a very good friend of mine. We love working on broken junk together. Thanks for watching!

  • @125southernnh2
    @125southernnh2 Рік тому

    Had a '67 wagon after high school. Slept in the thing.

  • @buffplums
    @buffplums Рік тому

    Some great music …

  • @roseymalino9855
    @roseymalino9855 Рік тому +2

    That mess on the rockers and push rods was sludge residue. One of the first jobs I had back in the '60's was cleaning / desludgeing a V8. Detergent oil wasn't yet popularized and engines were very prone to sludge formation especially if they didn't run a hi-temp thermostat and worse if they did short trip driving which contributed to internal engine condensation. Old timers back then would periodically do a kerosene flush before oil changes where we added a qt or so of kerosene and ran the engine 15 - 20 mins before the oil change. Stop laughing; I'm serious. Eventually the engines would lose oil pressure. The upper part of the engine was so sludged the oil galleys clogged preventing the oil from returning to the pan.

  • @scottnyc6572
    @scottnyc6572 Рік тому

    You’re in good hands with Mustie1.

  • @WAVEGURU
    @WAVEGURU Рік тому +1

    The movie you were thinking of is Flight of the Phoenix.

  • @JacobJosephVanStraten
    @JacobJosephVanStraten Рік тому +3

    Just start by removing the motor and cleaning and rebuilding it. It can be saved. No faith for a numbers matching car.

    • @driveanalog747
      @driveanalog747  Рік тому

      Yes this is an idea. I like the numbers matching part. Thanks so much for watching

    • @johnstrohsnitter2094
      @johnstrohsnitter2094 2 місяці тому

      Fords of that vintage did not have part of the VIN engraved into the engine like GM did, so any 66 whose casting number is the same and whose cast-in date code was close will do. The Falcon / Fairlane / Mustang / Fairmont 200 Six was a durable engine. The integral intake manifold made carb hop-ups difficult, but I believe that Edelbrock made a 3 carb conversion kit that really brought that engine to life. Had to take the head to a machine shop to drill 2 new ports and mill flat spots on the manifold to mount the kit. The engine was produced until 1983 or so. I don't know if it ever had port fuel injection but if not, it did have central fuel injection in its last year or 2 of production.
      Had an early70 Falcon wagon with a 302. great car, but when I got a company car and my wife got pregnant, I had to upgrade to a 78 Fairmont wagon with a 302. An even greater car. Saw the falcon 5 years after I sold it (Knew it was mine by the rust and the started repair, as well as the ornaments I pit on the grille. I sold that car with 145K NY Metro area miles to a guy who was commuting into the city with it. I bet he got the car to 200K miles.
      BTW, from 66 thru 70, the Falcon and Fairlane had similar wheelbases, especially the wagon. The 66-70 Falcons were Fairlanes with only 2 headlights. After Jan, 1070 (Mine was Aug 1969), they started slapping the last of the Falcon insignia on stripped down Torinos.

  • @fanofoldfans9238
    @fanofoldfans9238 Рік тому

    It was The flight of the Phoenix... Mustie1 good to see you getting greasy again!

  • @chrisssmallengines7163
    @chrisssmallengines7163 Рік тому

    The older engines built so well that even if you never change the oil they still run .

  • @utforskaren3031
    @utforskaren3031 Рік тому +1

    I want to see if you could get it to rotate around What does it take to get it to go around even though it's junk Would be possible if you could make a short clip about it or maybe could do an autopsy on it video on it How bad it looks inside the engine😋

  • @CharlesM-dp4xe
    @CharlesM-dp4xe Рік тому

    Flight of the Phoenix with Jimmy Stewart . Yeah I remember that. Too bad about that engine though.

  • @davidsnyder2000
    @davidsnyder2000 Рік тому

    AAAAHH! After all the hard work that motor needs everything. I can’t figure out how that motor could’ve gotten so much rust inside. That’s crazy. I’ve never seen one that bad in person. Car wad in a barn with a hood over sitting in an engine bay. Just doesn’t make any sense.

  • @stephenhunter70
    @stephenhunter70 Рік тому

    What series of (Aussie) Ford falcons had the 351 ci engines?

  • @ctiley2212
    @ctiley2212 Рік тому

    Those hideous things were so weakly built that in Australia they had to put large braces from the firewall to the strut towers to stop the whole front from collapsing, which along with all the other dangerous elements and sub standard parts made it a real widow-maker. The way they designed the braces made any maintenance a nightmare, trying to work around a cheap fix.