4L60E Autopsy - No Movement Mystery

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  • Опубліковано 24 бер 2024
  • I received this 2010 4L60E out of a Chevrolet Colorado where the primary shop's customer advised of an intermittent no-movement condition. The owner had the truck towed to the shop where the tech was able to pull it into the bay under it's own power and could not duplicate the no-movement condition.
    I tear down and inspect the transmission, trying to determine what may have caused the lack of movement the customer had reported and discover a few other things along the way.
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КОМЕНТАРІ • 31

  • @bobvandusen1832
    @bobvandusen1832 Місяць тому +1

    Very very good job!

  • @jayvalentin018
    @jayvalentin018 4 місяці тому +1

    Just wanted to say i appreciate the videos you put out especially being a smaller channel. All i have is transmissions from the GM Platform and you’ve helped out a lot.

    • @nickstransmissions
      @nickstransmissions  4 місяці тому +2

      Thanks, Jay! Hoping to become a 'bigger channel' soon. Glad my videos are helping you with your transmission work!

  • @notanotherslotguy
    @notanotherslotguy 4 місяці тому +1

    Great video as always! Keep them coming!

  • @wilburnmiller1851
    @wilburnmiller1851 4 місяці тому +1

    Great job

  • @yohanathandowns9057
    @yohanathandowns9057 2 місяці тому +1

    Subbed. Great work

    • @nickstransmissions
      @nickstransmissions  2 місяці тому

      Thank you for the kind words and subscription, Yohanathan!

  • @CleanCutLawnsK2
    @CleanCutLawnsK2 4 місяці тому +1

    Great video, Nick. I'd suspect the intermittent "no movement" condition was caused by all that clutch mud clogging the filter. After it sits a while, enough of it falls back into the pan that it will move again for a while, until it clogs up again. I'm like you, though, I always play doctor with each one. Gotta find the actual cause or it bothers me. Also, if you don't mind me asking, what kind of hot tank washer do you use? I'm in the market... I'm still cleaning everything by hand in a small solvent tank, but I've gotten busy enough now I think I can justify the time savings a hot tank would give me. I need a small one, though, as I have limited space.

    • @nickstransmissions
      @nickstransmissions  4 місяці тому

      Thank you, Kevin! I agree about the clogged filter, and that occurred to me a few days after I shot and produced the video, haha. Another commenter mentioned the same thing and think you're both correct.
      My parts washer tank is an old one and will be replacing it soon - I'll reply back later with the brand/manufacturer.

    • @nickstransmissions
      @nickstransmissions  4 місяці тому

      My hot tank is an old EMC brand washer, they still make them AFAIK...Here's their website: www.equipmentmanufacturing.com/parts-washer-powerjet-home.html
      My particular model has long since been discontinued but one of the two smaller ones may be of interest...My washer does a good job but it's getting very rusted out so looking to replace vs trying to repair it..I think it's at least 30 years old at this point, runs on 110 volt outlet power.

    • @CleanCutLawnsK2
      @CleanCutLawnsK2 4 місяці тому

      @@nickstransmissions Thanks. I appreciate it.

  • @douglash3129
    @douglash3129 4 місяці тому +1

    Hi Nick, I have been wondering why couldn't you use hex flange bolts to hold the bell housing on ,is it clearance or am I missing something?? Thanks for the video Nick!

    • @nickstransmissions
      @nickstransmissions  4 місяці тому

      Hi Doug, my guess is hex bolts of the appropriate height/depth would interfere with the torque converter so a female engagement design was used, and the TP50 bolts would frequently strip so they went to Mortorq in 2007 or 2008.

  • @frankdatank7751
    @frankdatank7751 Місяць тому +1

    Great work, love the videos!!! Ive been looking at some bushing drivers for the 4l60e, would the plastic bushing drivers work???
    Thanks!!!! They are a bit cheaper?????

    • @nickstransmissions
      @nickstransmissions  Місяць тому

      Hi Frank, thanks for the kind words! Those plastic/3D printed bushing drivers are fine for once in a blue moon but wouldn't trust them for regular duty use.

    • @frankdatank7751
      @frankdatank7751 Місяць тому +1

      @@nickstransmissions Awesome 👍 Thanks

  • @rust_hoarder_garage
    @rust_hoarder_garage 4 місяці тому +1

    I have a 65E doing the same thing, thought is the converter clutch material plugged the filter. Trans will work for a short time the first time the engine is started, then as soon as it runs a little while all gears go away as the filter plugs up. Will know for sure once I tear it down.

    • @nickstransmissions
      @nickstransmissions  4 місяці тому

      Thanks, rust-hoader-garage! I believe you're correct in that clutch material was clogging up the filter causing no movement...Yes, please let me know what you find once you tear the trans down.

  • @user-co3ul8sq4j
    @user-co3ul8sq4j 4 місяці тому +1

    if first gear not working must be the dirt clogged the oiling system

    • @nickstransmissions
      @nickstransmissions  4 місяці тому

      Yep, the consensus is that the TCC clutch material clogged the filter and caused the intermittent no movement condition.

  • @LarsonFamilyFarm-LLC
    @LarsonFamilyFarm-LLC 4 місяці тому +1

    Cativating disaasembly-enjoyed it. Shouldn't that "68" embossed end-play washer be put on w/68 face down? I remember you saying that in a 700R4 rebuild...I've been putting the stamped numbers down for less bearing wear.

    • @nickstransmissions
      @nickstransmissions  4 місяці тому +2

      Thanks for watching, KtF! Yep, you're correct - the numbers should be facing the drum not the bearing though I've torn down numerous units with that spacer in wrong and haven't observed any ill effects but the technically correct orientation is number-down.

  • @jaz11350
    @jaz11350 4 місяці тому +1

    Great video ... our you going to do a video on the vb tare down

    • @nickstransmissions
      @nickstransmissions  4 місяці тому +1

      Thanks, Jaz. Not doing any more 4L60E VB tear downs as I have those on the channel already and the only difference between the 09+ valve bodies is the lack of a 3-2 control solenoid and valve/spring. Everything else is the same insofar as the valve trains are concerned.

    • @jaz11350
      @jaz11350 4 місяці тому

      I was just wondering if maybe the afl valve was a issue but still don't explain why it was random 🤔 I have seen input drums test good when cold but leak after operating temp

    • @nickstransmissions
      @nickstransmissions  4 місяці тому

      Others have suggested a clogged filter insofar as the mysterious 'no movement' condition which makes sense given how the TCC disintegrated so likely jammed up the filter at times. The AFL valve wouldn't cause no movement but would cause 3-4 clutch burn up as well as other drivability symptoms.
      In the case of this transmission, the TCC regulator valve was really worn out (one of the worst I've seen in recent memory) so that contributed to the TCC failure. I put a Fitzall TCC reg valve in that thing which I did film so you'll see that in the coming days...I also filmed the vacuum testing of that valve body where you see the weakness in the AFL and TCC valve as well as the forward abuse bore plug...Pt 2 shows the fixes and re-test...
      All those videos will be on the channel by this time next week!

  • @AB-gi9gu
    @AB-gi9gu 4 місяці тому

    What would make one of these pull forward in both reverse and neutral, and all forward gears seem to work correctly? I expected to find the forward clutches welded together but they are in good shape. Very little metal in pan. I have the pump and the input drum out, but decided to stop there and do a little research. Can't seem to find anyone who has had this issue. This was not after a rebuild, just happened one day. Thanks for any insight.

    • @nickstransmissions
      @nickstransmissions  4 місяці тому +1

      Thanks for watching, A B...Sounds like possible cross leaks somewhere, perhaps between the valve body, spacer plate and case but odd that it developed suddenly after the transmission has a history of working normally. One other thing it could be is a collapsed forward thrust bearing, the resulting additional room for the drum to travel is allowing oil to get in behind the piston and allow it to apply...Also check the little bleed orifice in the forward piston housing to see if it's working and venting fluid...If not, that's your problem.