RIP BRC 500 😩

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  • Опубліковано 25 сер 2024
  • Ops 😅😅

КОМЕНТАРІ • 176

  • @dr.hugog.hackenbush9443
    @dr.hugog.hackenbush9443 4 роки тому +6

    100 octane fuel, Klotz castor at 40.0:1, and jet on the fat side for constant wide-open cycles. Maintain your air filter like a madman. Ive ridden and built 2-strokes for over 30 years and have never had an engine failure. You might want to consider a steel sleeve liner for your cylinder too. Just make sure you bring it up to temperature and break it in properly before you start hammering it. An old team Kawasaki Baja trick was a handlebar mounted choke to richen the mixture while riding, and that might be an option here as well.

    • @gnagsaar_
      @gnagsaar_  4 роки тому

      Dr. Hugo G. Hackenbush This is my first engine failure since 2005 😝 The issue here was cold pinch due to the missing thermostat and it turns out these cylinders was never intended to be tuned, for tuning they use a different cylinder/piston clarance (I have matched that now)

  • @jamessaitama5753
    @jamessaitama5753 4 роки тому +90

    Kikaninac dans quelques mois

    • @Junzo855
      @Junzo855 4 роки тому +1

      J'ai pensé la même chose mdrr

    • @isernarnaud2203
      @isernarnaud2203 4 роки тому +8

      Vu le montage sans aucune prise de côte , réglage de carb ect , c’est possible ...

    • @mateogentes4433
      @mateogentes4433 4 роки тому

      Obliger mdr

    • @turbolescargot2838
      @turbolescargot2838 4 роки тому

      Grave 😂

    • @CrownVL
      @CrownVL 4 роки тому +7

      Il se fout de notre gueule à dire « je suis le premier à faire ça à Europe ? »

  • @gusperf3454
    @gusperf3454 4 роки тому +47

    Espérons que Kika nous fasses pas la même , en sueur devant cette vidéo 😆

    • @34yannis
      @34yannis 4 роки тому +1

      Je croyais que c'était le seul en Europe a l'avoir fait 🤣👍

    • @shadowsbike1958
      @shadowsbike1958 4 роки тому

      @@34yannis Quand il a dit ça, c'était en 2018-2019, il la dit lors qu'un Live que sont projet à commencer en 2018 et certain moment de vidéo sont tourner en 2019

    • @Arthur-kk2eb
      @Arthur-kk2eb 4 роки тому

      NARVALUX MOTORBIKE c’est fort probable il a tout monté sans rien calculer... c’est pas des lego c’est de la précision un moteur

    • @CaptainDangeax
      @CaptainDangeax 4 роки тому +1

      @@Arthur-kk2eb Je pense que c'est plutôt un problème de graissage quand il a coupé les gaz. Plus de gaz, plus d'huile.

    • @weedytc73
      @weedytc73 4 роки тому

      @@CaptainDangeax Quand il a coupé les gaz ?
      Moi j'aurais dit mauvais rodage pour que le truc dur même pas 1 mois 😂

  • @znormand3690
    @znormand3690 4 роки тому +14

    How many hours/kilometers? If not a lot I think the likely cause is a wrong mix. Also be careful with the oil quality... I tested ipone and motul : piston was perfect at replacement step with motul, but with ipone oil the piston was dirt (with same running hours, kind of roads).
    Good luck!!

  • @valentinjougier3366
    @valentinjougier3366 4 роки тому +19

    Nan tant que sa arrive pas a notre kikaninac-_-

  • @IncuboUnconventionalLife
    @IncuboUnconventionalLife 4 роки тому +8

    Never give up 💪💪💪

  • @agustinizacelaya3465
    @agustinizacelaya3465 4 роки тому +13

    More mix!!!!! 4sure such a gripped cylinder in 2strokes are about pour gasoline it was running lean

    • @sashabanchi8679
      @sashabanchi8679 4 роки тому

      Oil mixture is not related to running an engine lean or rich.

    • @agustinizacelaya3465
      @agustinizacelaya3465 4 роки тому

      I’m not talking about fuel/oil
      I’m talking about gasoline/ air

    • @fab9727
      @fab9727 4 роки тому

      @@sashabanchi8679it is related but not that big of an impact. if you have more oil in it, it's less gas compared to air. So it definetly makes a difference wheter you run 6% or 2% oil mixture with the same carb setting.

  • @riccardomarzotto7974
    @riccardomarzotto7974 4 роки тому +14

    Never use engine brake on two stroke

    • @tsx2582
      @tsx2582 4 роки тому +2

      it was not the cause

    • @Aint1S
      @Aint1S 3 роки тому

      @@tsx2582 lol no kidding! 🤔 That would be the same as not revving the engine up and letting it idle back down...
      I forgot to say, *I agree with you!*

  • @manutexier8516
    @manutexier8516 4 роки тому +3

    Serrage au 4 coin dilatation piston excessif ( trop d’avance à l’allumage ou piston côte trop grande )

    • @MK4TDI115
      @MK4TDI115 4 роки тому +1

      Manu Texier 4 coins=surchauffe en général

    • @manutexier8516
      @manutexier8516 4 роки тому

      Oui mais il est important d’en s’avoir la cause !

  • @Aint1S
    @Aint1S 3 роки тому +1

    That's not the fault of BRC. Whew! I'd talk to the shop on the ring spec they mic'd them at.

  • @yohanvrff4016
    @yohanvrff4016 4 роки тому +7

    Kikaninac va pleurée je pensse bien 😭😭😂

  • @CaptainDangeax
    @CaptainDangeax 4 роки тому +1

    I seized my KMX125 30 years ago the same way. I was running full throttle on the highway, a car pulled over just in front of me, I cut the throttle and applied the brakes, and when I opened the throttle again, the engine seized. What happened ? When cutting throttle, no oil is pumped into the engine anymore. Therefore seizure. It's as easy as that. Now I've learned to drive a bike and always keep a minimum of tension in the throttle cable, and also I'm driving a 4 stroke 4 cylinder 1000cc bike now. Full throttle on the highway is not possible anymore.

  • @drspatzlescowboy7372
    @drspatzlescowboy7372 4 роки тому +3

    Im very sure, you were that guy on instagram spamming under every 300cc picture: "Buy a BRC 500 kit, its the best"

    • @gnagsaar_
      @gnagsaar_  4 роки тому +2

      D'r Spätzlescowboy Still is 🤣 this is me pushing the engine WAY longer than it was built for😝 I rode the stock BRC all last season

    • @yetzbiker4995
      @yetzbiker4995 4 роки тому

      @@gnagsaar_ it is better but waaaay less reliable

  • @victorhogvall2065
    @victorhogvall2065 4 роки тому +3

    This exactly happend to my moped after i put on a high rpm exhaust (vocca warrior) om My 75cc I went full throtle and went about 120 km/h and it just died

  • @GiacomoTrombetti
    @GiacomoTrombetti 4 роки тому +4

    Some break-in?

  • @cristianr3712
    @cristianr3712 4 роки тому

    Great content, keep it coming! Please buy an EGT and make sure to use it while riding, that way you´ll know when to stop pushing he bike before something happens.

  • @mattlennymoore282
    @mattlennymoore282 4 роки тому

    Main jet or piston ring end gap was incorrect. Possibly oil mix ratio but surly you got that right with a 8-10k engine?

  • @baby-sharkgto4902
    @baby-sharkgto4902 4 роки тому +1

    Impatiently waiting..... good luck bro

  • @nick4506
    @nick4506 3 роки тому

    wow normally when I blow up a twostroke it's the piston skirt cracking off and embedding metal into the head. but this was the cilender plating chipping off first maybe its a BRC issue.

    • @gnagsaar_
      @gnagsaar_  3 роки тому

      Yeah, I heard from others who seized too. U can't go full throttle on these. After 6800rpm the power signs out and all you do is superheat the piston and the engine "cold pinch seizure"

  • @RebelBmxCrew
    @RebelBmxCrew 3 роки тому

    Can’t trust these Canadian companies anymore. My panthera electric start kit is garbage I have so many issues with it

    • @gnagsaar_
      @gnagsaar_  3 роки тому

      yeah 😒 sorry to hear that 😬 if it helps, the electric starters on brc lasts like 10hr of riding 😂 and with only re-starting an already hot engine😝

  • @unusualsuspect1262
    @unusualsuspect1262 4 роки тому +4

    Ouch... Bad image for brc

    • @Di4b0LlK
      @Di4b0LlK 4 роки тому +1

      2T depends more of the driver and the guy who mount the motor

    • @lauri.lyijymaali
      @lauri.lyijymaali 4 роки тому

      Two strokes just are like this if everything isn't correct.

  • @followtheciaence
    @followtheciaence 4 роки тому +1

    Please post some street ride videos of this bike, I'm not seeing anything. Thanks

    • @gnagsaar_
      @gnagsaar_  4 роки тому +1

      Charles S later for sure 👌

  • @MOTO_MAVERICK53
    @MOTO_MAVERICK53 4 роки тому

    Lol like it how you have music to cover the sound off your bike fucking up because you haven’t used a big enough mix

  • @anlonning
    @anlonning 4 роки тому +1

    Kondolera. Men godt du ikkje gir deg på an

    • @gnagsaar_
      @gnagsaar_  4 роки тому

      AndyLonn Lere kanskje nåke av da 😝 neida, va uforsiktig

  • @MXUnion
    @MXUnion 4 роки тому

    Cool!

  • @Di4b0LlK
    @Di4b0LlK 4 роки тому +2

    maybe you drive without enough oil mix

  • @jmakinen.
    @jmakinen. 4 роки тому

    U should have at least 4% mix in that machine

  • @Aint1S
    @Aint1S 3 роки тому

    That top ring wasn't right at all. Mic and check it. Looks like it wasn't slipping, but scuffing to scraping the walls as if it were a 4T.

  • @colonelguil
    @colonelguil 4 роки тому +21

    Tous sec au démontage.....

    • @MrAnthony62450
      @MrAnthony62450 4 роки тому +1

      exact , c'est sec tout SEC !! ahhh ma fois un tio pastis c'est pas d'refus ...

    • @celestinschermann5927
      @celestinschermann5927 4 роки тому +3

      Mr Golden le moteur à pas été bien lubrifié donc pas d’huile donc serrage

    • @celestinschermann5927
      @celestinschermann5927 4 роки тому +2

      Mr Golden oui ou si il a une pompe à huile (je crois pas) la pompe à huile est tombé en panne donc mauvais mélange ou mauvaise huile

    • @colonelguil
      @colonelguil 4 роки тому +4

      @@celestinschermann5927 il est au mélange et sûrement une mauvaise huile ou alors il n'as pas assez mélangé car il a serré quand le moteur etait en charge a fond

    • @celestinschermann5927
      @celestinschermann5927 4 роки тому +1

      Ugo Hiel ouais mais dans tt les cas rip psk il vas devoir vendre un rain après avoir vendu sont bras pour acheter le kit ptdr

  • @robbed_of_sanity
    @robbed_of_sanity 3 роки тому

    The engine fell below operating temperature is what I'm guessing. Cold seizure for sure

    • @gnagsaar_
      @gnagsaar_  3 роки тому +1

      It did "cold pinch", but not because dropping in temperature. To quote BRC: "our kit was never design to produce power over 6800rpm" I know NOW that if you ride this engine over 6800rpm it drops fast in power and it causes the piston to heat up fast insted. ALOT of ppl have seized these, I was just filming when I did. IMO this is a prototype engine that should never have been sold to the public.

    • @robbed_of_sanity
      @robbed_of_sanity 3 роки тому

      @@gnagsaar_ we call it a cold sieze here in the states.

  • @laysstandard
    @laysstandard 4 роки тому +1

    ah another youtube video i leave muted the entire time. great.

  • @jalluisbest2374
    @jalluisbest2374 2 роки тому

    Wdym "sorry headphone users"? More like bless the headphone users🥵

  • @tristantee8187
    @tristantee8187 4 роки тому +1

    Would look into the cause before just reassembling once new piston and plating.

    • @gnagsaar_
      @gnagsaar_  4 роки тому +2

      Tristan Tee Yeah ofcorse, gonna do counter messures to EVERYTHING that could have been wrong 😝

  • @KuhKronus
    @KuhKronus 4 роки тому

    Well, at least you got $500.

    • @gnagsaar_
      @gnagsaar_  4 роки тому

      Sully It would cover the costs of the cylinder repairs 🤞🤞

  • @julesm3654
    @julesm3654 4 роки тому

    Yo hi, schade, dass ich dir bei deinem Projekt voll und ganz unterstütze, auch wenn dein Motor kaputt gegangen ist ... Ich bin ein Franzose, der dich zufällig mit deinem 500 BRC auf Instagram entdeckt hat und ich habe gerade deinen UA-cam-Kanal entdeckt. Zwinge dich.

    • @marbinchen1991
      @marbinchen1991 4 роки тому

      why do you write in german when you are french tf

  • @galanofgaia2881
    @galanofgaia2881 4 роки тому

    Have they improve on plating with ceramics yet???

  • @timpo4568
    @timpo4568 4 роки тому +1

    Are you going to rebuild it?

    • @gnagsaar_
      @gnagsaar_  4 роки тому +3

      timpo r YES 😉 even better 👌

  • @450rmzouave4
    @450rmzouave4 4 роки тому

    7500$ pour que ça finisse comme ça.. ça doit faire mal au cul

  • @ibnelfaismahdi1871
    @ibnelfaismahdi1871 4 роки тому +3

    7500 $ is gone 🙂

  • @momobylette72
    @momobylette72 4 роки тому +1

    no no no what

  • @larsloopmans7280
    @larsloopmans7280 4 роки тому

    Probably not enough fuel or not rich enough premix

  • @ronxdriver
    @ronxdriver 4 роки тому

    I suggest you to get a proper carburator, i may be wrong, but newer ktm's Has the 36 carb. Maybe you should get a 38 or even a 39 with some proper jetting. The 500cc draws a lot more air volume. Or even better a lectron carb, but not just plug and play one, one that is properly jetted for supermoto, wideopen cycles.

    • @volvo855t2
      @volvo855t2 4 роки тому +4

      Ron Shteiner he talked about it on instagram and that he had tested the lectron but it didnt work well with the setup he has

    • @ronxdriver
      @ronxdriver 4 роки тому

      Didn't know that. 😬 in any case those "huge" bores in a super moto use will be surely less fragile if ran on a little bit richer mixture, surely be better leaving the "lean" spot on mixture for 125cc's

    • @gnagsaar_
      @gnagsaar_  4 роки тому +3

      Ron Shteiner I tried both lectron 38 H series and a lectron 40mm. But it seemed like i had to choose between easy start or power 😂 The middle thing was just "meh" fuel range was good tho 😝 atm I have a 36keihin bored to 39,3mm thats 100% as big as my reed will allow as for size. If you just messure the diameter x 3,14 on carb and backwards messuring it on the intake/ reed opening. BUT In Adam Miller is working on his BRC 500 now, so I'm pretty sure he will come up with the PERFECT carbsetup 😝

    • @ronxdriver
      @ronxdriver 4 роки тому

      @@gnagsaar_ good to know.
      Your project is awesome, hope to see some major updates soon.
      BTW what jetting parameters you ar running now?

    • @gnagsaar_
      @gnagsaar_  4 роки тому +2

      Ron Shteiner There will ba a wait intil i get the cylinder back atleast, but weight reduction is still going 👌 Reached 99,53 KG today👌 jetting was to BRC spec + some more, but I'm thinking that I'm gonna go WAY up on the mainjet, and jet downwards til it does not drown next time😂 to be 100% sure😂

  • @mandonini_
    @mandonini_ 4 роки тому

    More problems than riding

  • @anto-rp7ej
    @anto-rp7ej 4 роки тому

    Le temps que kika la pas ses pas grave

  • @bena8725
    @bena8725 4 роки тому +1

    Bon ben RIP😂

  • @gaboydodier
    @gaboydodier 4 роки тому +1

    Bad jetting and need more oil

  • @Samib.a
    @Samib.a 4 роки тому

    Sounds like 50cc

  • @henriksgarage2049
    @henriksgarage2049 4 роки тому

    Er den godkjent på norske veier?

  • @marceauhgr4928
    @marceauhgr4928 3 роки тому

    Kika tremble 😂

  • @tinou18
    @tinou18 4 роки тому

    voilà pourquoi il faut faire régler votre moto par des pros

  • @Yoniproject__
    @Yoniproject__ 4 роки тому

    Kika en sueur

  • @sachaperard2381
    @sachaperard2381 3 роки тому

    Envoie le a airsal

  • @markbaxter8188
    @markbaxter8188 4 роки тому

    Are we at 70 rwhp yet?

    • @gnagsaar_
      @gnagsaar_  4 роки тому +1

      Mark Baxter Can't be far off atleast, the power is sick next to the stock setup 👌 right now not so much tho😂 4-6weeks from now we can try again

    • @markbaxter8188
      @markbaxter8188 4 роки тому

      @@gnagsaar_ I have been looking forward to the video following the porting and bored carb. And alternative pipe to the stock supplied FMF
      I see BRC are doing new CDI units now.

    • @gnagsaar_
      @gnagsaar_  4 роки тому

      Mark Baxter Yeah I struggled a bit with motivation for YT 😝 My edits up til now have just been getting like 1k views while my instagram story gets 4k views 😂 But I might try to make a better video while rebuild 😝 YT has missed out on ALOT 😝

  • @gulag_dt
    @gulag_dt 4 роки тому

    Leipo:d

  • @TheEpiphone2
    @TheEpiphone2 4 роки тому +2

    7500 € pour ça 🤣 en espérant que se qui avait l'intention de faire la même chose (installer le kit brc ) on changé d'avis . Bah oui c'est pas parce que des "youtuber "qui fond des vidéo sur un produit que se produit est forcément une pépite..

    • @Drivewatch
      @Drivewatch 4 роки тому +1

      Oui enfin le produit si il est mal monté ou mal réglé ... n’importe quel cylindre peut serrer.

    • @TheEpiphone2
      @TheEpiphone2 4 роки тому

      Non jure ...🧐

    • @sambal4338
      @sambal4338 4 роки тому +1

      pas la faute du cylindre tu serre rarement a cause de la qualité du cylindre le montage esr hyper important

  • @bricebeguet9223
    @bricebeguet9223 4 роки тому +1

    Enlève ta musique on entend rien au début

  • @HARDSenSaTion
    @HARDSenSaTion 3 роки тому

    that why i hate 2 stroke engine

  • @undisturbednaturalworldd3102
    @undisturbednaturalworldd3102 4 роки тому

    noizii --

  • @ThePhyfa13
    @ThePhyfa13 4 роки тому

    Nooooo

  • @lecrafteurdu14
    @lecrafteurdu14 4 роки тому

    I think overheating, the nikasil is lifted of

  • @jeanmim66
    @jeanmim66 4 роки тому

    How many hour your engin ?

    • @gnagsaar_
      @gnagsaar_  4 роки тому +1

      Jean mi M 51ish hrs, this was 1,5 hrs after tuning 🤣

    • @jeanmim66
      @jeanmim66 4 роки тому

      gnagsaar moto sorry for my bad English I’ m french, 51 hours your engin before it break ?

    • @mat-mat_englisse
      @mat-mat_englisse 4 роки тому +2

      Jean mi M en gros son moteur avait 1 h 👍🏼

    • @overdrive9739
      @overdrive9739 4 роки тому +1

      Matteo Sordillon, je crois qu'il a 51h et qu'il a fait ds ajustements vers 49h30....

  • @jasonjaeger4042
    @jasonjaeger4042 4 роки тому

    That sux man

  • @kittipongkanphet5096
    @kittipongkanphet5096 4 роки тому

    ไส่มันทูทีมั่งต่ะบาว

  • @supreme7488
    @supreme7488 4 роки тому

    6000€ dans le cul ça fait mal ptdr

  • @simonyap6426
    @simonyap6426 4 роки тому

    95kg 😳

  • @SuperEirik12345
    @SuperEirik12345 4 роки тому

    Har du fortsatt tsx'n?

    • @gnagsaar_
      @gnagsaar_  4 роки тому

      Birkeland nope, såg den til salgs på en fb gruppe i fjord tror eg, urørt siden eg hadde den 😝 bare litt meir rust

    • @SuperEirik12345
      @SuperEirik12345 4 роки тому

      @@gnagsaar_ Så den lever enda altså

    • @gnagsaar_
      @gnagsaar_  4 роки тому

      Birkeland verfall som en sylindret, veitkje om dei har fått den til å virke igjen med to 😝

  • @JoeRoganClipsss420
    @JoeRoganClipsss420 4 роки тому

    Du greier å fikse alt mulig da greier du dette

    • @gnagsaar_
      @gnagsaar_  4 роки тому

      Suzki bare et spørsmål om tid 😝

  • @steffentysnes5302
    @steffentysnes5302 4 роки тому +3

    Get it bored to 550, or buy a maico 700cc engine..

    • @jj-hf8jy
      @jj-hf8jy 4 роки тому

      You clearly dont know this setup. This engine is built for this ktm and will require 0 rigging up to install and has a counterbalancer&electric start. It would be downgrade to move to maico.

    • @steffentysnes5302
      @steffentysnes5302 4 роки тому

      @@jj-hf8jy this engine was in another bike before, and it's not like it's the end of the world to make some new engine mounts, and I'm guessing there is some balancing parts in the maico as well, but sure, let's go with your thoughts

  • @ItsAikos279
    @ItsAikos279 4 роки тому

    cheh !