Seized LiFan Generator (Part 1) - What Happened?

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  • Опубліковано 6 січ 2025

КОМЕНТАРІ • 293

  • @warrantyvoid100
    @warrantyvoid100 3 роки тому +23

    Scotch-Brite the crank journal, run a hone through the con-rod 'til it fits, use the torque specs from whatever that's a clone of, put the oil back in and send it.

    • @oldsranch
      @oldsranch 3 роки тому +2

      nothing to lose, right!

    • @davidkettell5726
      @davidkettell5726 3 роки тому +6

      i once took out a lot of wear in a con rod by machining down the cap ang used Prussian blue and a scraper to refit it . The engine ran good for two more years and then i sold the tractor

    • @YodaWhat
      @YodaWhat 3 роки тому +1

      Yes, it definitely seems like the connecting rod's _big end clearance_ is about zero. But did the generator come that way from the factory? Or was it already rebuilt, with incorrect parts?

  • @mikesbarn1858
    @mikesbarn1858 3 роки тому +27

    My suggestion would be to clean the crankshaft and hone the con rod then use plastic gage to get your.003 clearance. I noticed that the piston skirts seemed a little tight also.

  • @idontneedaname85
    @idontneedaname85 3 роки тому +12

    I’m excited to see a rebuild.
    There is very few things in life as cool as watching an engine start for the first time after a rebuild.

  • @homesummy8034
    @homesummy8034 3 роки тому +20

    Seems to be a common pattern. Oil runs low, and the rod fuses itself to crank. In this case, the operator heard it happening and stopped the engine before the rod broke, but most of the time, it just runs until the engine flies apart internally.
    From all of your videos that I have watched, I have picked up and learned many things, but the top of the list of things I've learned is to KEEP THE OIL FRESH AND FULL, and always use synthetic oil! The second on the list is to drain the carb each time, keep the fuel fresh and use stabilizer.
    Because of you and your videos, I have completely changed the way I maintain my Predator 8750. Hopefully, because of you, it will last nearly forever.
    This LiFan engine looks identical to my Predator 8750. All of the Honda clones look pretty similar. I bet you could use the specs, and maybe even the replacement parts, from the Predator on this LiFan.
    Thank you James.

    • @williamvaughan1218
      @williamvaughan1218 3 роки тому +2

      Most importantly check the oil before starting because it might be fuel diluted.

  • @akhtarkh
    @akhtarkh 3 роки тому +1

    Honing the connecting rod or grinding the crankshaft would make for a nice rebuild video. No new parts repair videos are the most fun videos to watch.

  • @roy2689
    @roy2689 3 роки тому +1

    I agree with some of the comments below, polish the crank journal, clean up the con rod bearing till it's a nice fit on the crank, and rebuild ...

  • @whitesapphire5865
    @whitesapphire5865 3 роки тому +20

    An interesting little challenge! - I'd be looking at that big-end again and seeing if if can be made to live again. It doesn't look too seriously burned (but I am viewing on my phone), but with some care, all that abraded surface could be pared back and still reveal a usable surface which could well have remained in spec. The crank looks exceptionally good, considering what's gone on. This engine reminds me of a Fuji Robin 8HP diesel we had on a generator, and it had suffered much the same way. The guys at "Engine Reclaim" made an excellent job of renovating the rod - The crank was fine, and removing the tarnish from the piston skirt was all it needed to bring things back to spec.
    However, as we see "Pupp, popp, plooff, plopp, Popple pudd"!! You've already got it back together again, and something ain't right somewhere! - Timing? Or bad valves? Can't wait to see!

  • @robertfountain4856
    @robertfountain4856 3 роки тому +2

    Having a good laugh with this one because it makes me remember when I was young and foolish & I had a very similar problem. It was a rather old and battered genset but I needed it back and running so I honed the connecting rod. It freed up and was still a touch tight so I put it back together. 20 years later it is still sitting just behind me in full working order. Changed the oil after 30 minutes run and it now shows no sign of problems in the oil. Only used once or twice a year. It will probably outlast me.

  • @Tom-In-Ga
    @Tom-In-Ga 3 роки тому +1

    The teaser at the end was funny. Flames out the exhaust and intake. Can't wait for the next vid on this.

  • @bubbatime
    @bubbatime 3 роки тому +1

    A guy below recommended cleaning up the crankshaft journal and cleaning up the connecting rod as well. I would go this route. Some fine polishing sand paper (or whatever they use in machine shops), and go lightly. I bet before too long, you'll have a perfect fit.

  • @richardbaker3621
    @richardbaker3621 3 роки тому +1

    This one sure keeps my interest. I didn't notice any comments about low oil shut off. Please mention the presence or lack of in next video. Also your method for testing the low oil shut off so you can be certain its working before engine reassembly. Thanks for the video

  • @kens97sto171
    @kens97sto171 2 роки тому

    Lifan is a major manufacturer, they build engines for all sorts of things.. motorcycles, scooters etc.
    I was a bit surprised.. the build on that looked better than I expected, nice bearings supporting the shafts, a balance shaft, the casting on that rod and piston looked nice.
    I think I would try to hone it, and plastigauge it.. see if you can get it to loosen up.
    Usually when they run low on oil and seize up you will see some blue color on the parts that got hot.. either the owner caught it quickly and shut it down, or maybe there is a machining defect from the factory and it was just a bit tight on the clearances, it got a bit hot, parts expanded and it grabbed and locked up quickly.
    great video.. looking forward to part 2

  • @josephmello3819
    @josephmello3819 3 роки тому +2

    You are the best on you tube the only bad thing I see is you need a table to work on not on the floor . I hope to see you soon working on a table even if it’s just 2 horses with a piece of plywood. Thank you , you are the best

  • @lrrromicronpersei8294
    @lrrromicronpersei8294 3 роки тому +5

    As others have said work with what you have there if you cannot find a replacement.
    I would polish the crank then use some sharpie or similar to cover the big end on the connecting rod to see where it is dragging and go from there…..
    Keep up the great work..

  • @tiredoldmechanic1791
    @tiredoldmechanic1791 3 роки тому +9

    Use a micrometer to check the crankshaft to make certain that it is round then ream or hone the rod to match with clearance. You can get an adjustable reamer set that covers from 15/32 to 1-1/16 for $55 or one that goes from 15/32 to 1-3/16 for $83 on Amazon or get a single reamer that covers the size needed. Either one is cheaper than the new rod and you have them to use for other things. An automotive machine shop could also do it. Even a flap wheel might do a good enough job.

  • @AntonioClaudioMichael
    @AntonioClaudioMichael 3 роки тому +2

    Wow at how clean that cylinder looks

  • @hectorarroyo2285
    @hectorarroyo2285 3 роки тому

    Hello James. that engine is damaged that crankshaft may be twisted possibly. the best option is to fit a new engine with the same characteristics and get it running and worst case scenario use that generator for parts...thanks for the excellent generator diagnostic and repair tutorials...James Condon Academy.. .😁👍👍👍 greetings from Puerto Rico 🇵🇷...

  • @rosewhite---
    @rosewhite--- 3 роки тому +1

    Reminds me of old Triumph motorbikes that had the dural rod running direct on the crank.

  • @ni_wink84
    @ni_wink84 3 роки тому

    That’s trick for pulling the rotor is pretty good! I’ve heard of Irish spring soap in a crank to pull a pilot bearing but this is just as ingenious

  • @AntonioClaudioMichael
    @AntonioClaudioMichael 3 роки тому +2

    Makes sense it's the connecting Rod bearing surfaces aren't smooth no more and it's gripping the crank shaft

  • @johndean7618
    @johndean7618 3 роки тому +2

    Good job, but I might try lapping the con rod to the crank. I have done that before and had great success

  • @danhunik7949
    @danhunik7949 3 роки тому +1

    In trade school we were warned about putting bolt into holes with water or oil in them. Never thought I would see it put to a good use.

  • @lv_woodturner3899
    @lv_woodturner3899 3 роки тому +2

    I love the trick of using water and bolt to get the rotor off. I am amazed the connecting rod was not gauled since it was the cause of the lock.
    Looking forward to the next video.
    Dave.

    • @jcondon1
      @jcondon1  3 роки тому +4

      It’s the best looking bad connecting rod I have pulled out of an engine.

  • @guigamoretto
    @guigamoretto Рік тому +90

    We have used the ua-cam.com/users/postUgkxOTeIs0vv4_9B5hsmnLsk9r930uDQLu_Y for probably 30 hours with our camper and it’s been great! The noise level is really only noticeable when running the AC and other appliances like the microwave, hair dryer, or coffee pot. It’s not huge like other ones and it has wheels so even at 90lbs, I can move it!

  • @davidschipsi1316
    @davidschipsi1316 3 роки тому +3

    James, you always do the job right. Others have gotten good result working many times with what they’ve got. With some checking over and some fine hand work it looks like this engine can go back together with little to no new parts. Good luck with this challenge. Someone said it’s not rocket science. I’m a fan.

  • @brngrofdeth
    @brngrofdeth 3 роки тому +1

    Very nice work as always! Love and blessings from Ontario Canada!

  • @rickgaine3476
    @rickgaine3476 3 роки тому +5

    Nice job at a diagnosis. Will be interesting to see what you do with this in the future.

  • @ericvaughn1126
    @ericvaughn1126 3 роки тому +2

    Interesting state for this one to be in. Looking forward to seeing you get it to the point of the test start as seen in the teaser at the end!

  • @Mikesorrento3344
    @Mikesorrento3344 3 роки тому +10

    I like the nut on the flywheel trick to remove flywheel with hammer as opposed to gear puller. Also, the hydraulic removal of rotor is very cool. These Chinese clones are fun to work on. Parts cheap, unfortunately, these units don’t last. Sometimes you get lucky. I just sold a Champion generator that had over 1000 hours on the meter.

    • @dadskrej5226
      @dadskrej5226 3 роки тому +1

      Be very careful hammering on the crank nut while applying pressure to the flywheel to loosen it. It is easy to break the crankshaft...ask me how I know. Expensive!

    • @YodaWhat
      @YodaWhat 3 роки тому +1

      @@dadskrej5226 Also, it can destroy the ball bearings when that is what the crank runs on.

    • @jamesfranko5098
      @jamesfranko5098 3 роки тому

      they last if you look after them. most treat them like shit.

  • @jimthompson3030
    @jimthompson3030 3 роки тому +1

    i work on all things but from this video i will nottt look at these things!! to hard to work on i am far to lazy and smart to tackle these generators let it up to you for the punishment terrific video thank you!!

  • @watermanone7567
    @watermanone7567 3 роки тому +2

    Good video. Use plasta gage on the rod bearing to set the proper clearance. I think the valve rotator is missing on the exh. valve. Might try a percision expandable reamer for the rod bearing. Thanks for the video.

  • @aymannabil9
    @aymannabil9 3 роки тому +1

    Wow finally I saw one like mine.. this one will be interesting for me ...can't wait to see part 2
    U gonna do it Mr. James 👍

  • @arthurbiringer5676
    @arthurbiringer5676 3 роки тому +1

    You’re going to get it running!

  • @AntonioClaudioMichael
    @AntonioClaudioMichael 3 роки тому +3

    I do think the valves are apart of the issue Good video that stator put up a massive fight nice work getting it off without any casualties @James Condon

  • @AnwarKhan-dw8cj
    @AnwarKhan-dw8cj 3 роки тому +1

    go for it James use other genset torque values may have to polish crank journal use std clearances etc ,here in the tropics is polish clean up and assemble with just gaskit set

  • @ronaldkubert4527
    @ronaldkubert4527 3 роки тому +1

    My back hurts watching you work on the floor

  • @stazeII
    @stazeII 3 роки тому +8

    Was definitely not expecting a frozen rod. The way that piston fought being removed I expected to see a chunk of valve head wedged between the piston and cylinder.
    Glad you’re going to keep going on this one!

  • @larrysmith3374
    @larrysmith3374 3 роки тому +2

    Awesome timing! Just sitting down with my coffee.

  • @mickles1975
    @mickles1975 3 роки тому +2

    I wouldn't have thought of using hydraulic pressure to get that off. That's a neat little trick.

  • @duaneclarke7411
    @duaneclarke7411 3 роки тому +2

    Yep me to just sat down with a wild Turkey my guess connecting rod as you said it ran out of oil and the rod got hot and expanded and seized.
    great video's mate Thanks

  • @Lennyj24
    @Lennyj24 3 роки тому +1

    Ahh man, teasing with that little trailer at the end.

  • @davidblake6889
    @davidblake6889 3 роки тому +1

    I have just found your channel, James, and I am totally hooked! I wish I had had it available when I was doing light machine maintenance years ago. Your knowledge, patience and expertise is amazing. I would love to see the engine rebuilt. Like some other commenters, I think trying to lightly machine the crank shaft and big end to make them fit better would be a good first step. If that does not work, go for the new con rod.

    • @jcondon1
      @jcondon1  3 роки тому

      Will be publishing the rebuild tomorrow.

  • @Rorschach1024
    @Rorschach1024 2 роки тому

    James, a little trick when your puller jaws keep slipping off, put a large hose clamp around the jaws and that will help keep them on whatever you are trying to pull off the shaft.

  • @sferg9582
    @sferg9582 2 роки тому

    I love the water puller trick! Never saw that one before. Brilliant.

  • @martinflanagan2506
    @martinflanagan2506 3 роки тому +2

    I have saved buying many connecting rods , take 400 grit wet and dry sandpaper and W.D.40, carefully sand the rod bearing surface to nice new surface , do the same with the crank journal . Then plasti guage the fit to check clearance . It will save you $90.

  • @francisbailey3831
    @francisbailey3831 3 роки тому +1

    Hi James, yet another challenge for you. By watching your video's, you will solve the problem without any question as you always do. Will look forward to seeing you next video on the outcome of the engine.

  • @generessler6282
    @generessler6282 3 роки тому +1

    Maybe someone before you did a rebuild with an undersized rod, not knowing what they had. I'd mic up the journal and rod to see. If they never got it started, both could be usable, and you could get away with boring and/or lapping. It would be great to find a manual with factory sizes.

  • @davidcampbel
    @davidcampbel 3 роки тому +1

    Interesting disassembly, thank you for another entertaining video.

  • @wildefox1478
    @wildefox1478 3 роки тому +1

    Looking forward to the next video on this generator, I'm sure you'll bring it back to life, nice work as always!

  • @mjg263
    @mjg263 3 роки тому +4

    Very interesting failure! I wonder if it’s just a defective engine that didn’t have the tolerances quite right from the factory. Quality control seems to be all over the place with some of these manufacturers to say the least.

  • @christophermarshall5765
    @christophermarshall5765 3 роки тому +1

    The conrod assembly can be reused. Assemble the rod cap to the rod, & carefully hone it with a fine honing stone. Won't need much, or wrap p1200 wet & dry around a piece of timber just big enough to fit the rod assembly, & push it back & forth for about 30 seconds, using water to float the debris away. Test fit to the crank, oiling the rod assembly before testing.

  • @wazza33racer
    @wazza33racer 3 роки тому +2

    great thing about Aluminum rods is that they tend not to destroy the crank journal. Some hydrochloric acid and linish with wet/dry sand paper (spun with a shoe lace) and they can polish up like new. Spare rods are available online inexpensively. If you have a really non identifiable chinese clone engine............just measure the rods crucial dimensions and find one online that measures up.

  • @1bigsyd
    @1bigsyd 3 роки тому +2

    I love your videos..but please for my back and knees watching you…can you get a bench to work on please 🙏 😝

  • @Skynet-1
    @Skynet-1 3 роки тому +3

    Spoiler alert at end, nice. Looking forward to part 2! 👍👍👍

  • @TheIronDuke502
    @TheIronDuke502 3 роки тому +9

    James, I was really kind of wondering if maybe that this engine slipped through with little to no “Quality Control” when it was manufactured - Or Possibly A Monday or Friday Special.
    When I viewed this video, it was very apparent that engine parts were out of tolerance enough to bind up rather than totally seize once a abnormal heating condition manifested itself or as you alluded to with the air intake system drawing a large amount of dirt or maybe a combination of both situations.
    As some of the other comments alluded to, Some cleanup and or minor machining could possibly make all of the difference in the world with this engine - Barring no cracking or severe scoring has occurred.
    I have seen engines in far worse condition internally than ran like a sewing machine.
    James, I am really looking forward to seeing your follow up video regarding the engine situation. I am a retired welder/fabricator and had a 1954 Hobart engine drive welder that I occasionally had to clean the brushes on. It’s truly amazing how deeply that the Mud Daubers would build their nests in periods of inactivity of welding equipment. So naturally I am really drawn to your generator repair videos.from my past history of welding and maintenance of my welders.

  • @davewolf8869
    @davewolf8869 3 роки тому

    In my limited experience, lifan engines have been top quality machines.

  • @jp-um2fr
    @jp-um2fr 3 роки тому +1

    Ran out of oil and the big end picked up. Aluminium is not the best bearing material. If all else fails a half round bearing scraper and see if it cleans up.

  • @CrazyMan_Engineer
    @CrazyMan_Engineer 3 роки тому +1

    Would acid cleaning the crankshaft help. Also a light sanding of the Conrod bearing surface to get rid of glazing could help too.

  • @jeremydewolfe8026
    @jeremydewolfe8026 3 роки тому +1

    Just a note, out of the upmost of respect for you and your video editing sir! Obviously this will be a voice lost in a sea of voices however maybe it’s one more drop in the bucket. Would love to of seen you carefully remove the connecting rod from the crankshaft at the end of the video. Thank you for the content sir!

  • @gerardohernandez7401
    @gerardohernandez7401 3 роки тому +1

    Hey James! I had the same exact generator with the same exact problem, except mine threw the rod thru the casing. It’s literally a GX390 clone. I used a GX390 casing with a cheapo Amazon GX390 rebuild kit and it all went back together flawlessly.

    • @r8118830
      @r8118830 3 роки тому +1

      In the sales literature this generator engine is described as being 420 cc in capacity. Is it a 420 or a 390?

    • @jcondon1
      @jcondon1  3 роки тому +1

      This one is 420cc. Most GX390 parts will fit.

    • @gerardohernandez7401
      @gerardohernandez7401 3 роки тому +1

      @@jcondon1 mine must be older or different model, mine had a 389cc powercease engine.

  • @rhiantaylor3446
    @rhiantaylor3446 3 роки тому +14

    I have some experience of killing small engines like this. Mine was a 3 inch pump using a diesel engine. The issue was the splash-fed oil system which didn't like being left to run when located on an inclined slope. Oil cut-off doesn't help if that part of the sump is still full.

    • @GGigabiteM
      @GGigabiteM 3 роки тому +4

      It'd be nice if they had a tilt switch somewhere on the unit that would kill ignition if tilted over some degree range, but that'll never happen.

    • @r8118830
      @r8118830 3 роки тому +1

      @@GGigabiteM That would be very easy and cheap.

  • @johnhorsnell6410
    @johnhorsnell6410 2 роки тому

    Definitely try Scotch Brite and WD40 to remove scoring on bearing shell plus same on journal. suggest you use reassembly lube , refit bigend and check for smooth dragless rotation.

  • @richardcranium5839
    @richardcranium5839 3 роки тому

    i notice you pull the end housing off the generator first. i always pulled the rotor off and stator as a unit. i took an old bolt and cut it down for jacking the stator off with an m12 bolt . i found it easier to get that bearing out.

  • @deangentles4966
    @deangentles4966 3 роки тому +1

    Hi James my experience would be parts bin mate the challenge is to great with lots of your time with little money at the end and Thats if you get it working James looking forward to see what you will do mate

    • @jcondon1
      @jcondon1  3 роки тому +2

      The plan originally was to use it as a parts machine. But will try and get it going. The damage does not look bad.

  • @johncourtneidge
    @johncourtneidge Рік тому

    Here's the thing.
    This machine is identical to others that James has renovated. In other words, the manufactureres in China have been gradually been bought out such that the paint job might be different but nothing else is.
    This happened in the UK between 1960 and 1980 in the bus and coach industry: the phrase used for that homogenisation was 'Badge Engineering'.
    I experienced the same when I was setting up my kitchen in 2012: all kitchen knives has the same design and manufacture, save for different handles.

  • @TheStuffMade
    @TheStuffMade 3 роки тому +4

    Great video. Looks like it ran out of oil and everything got too hot, lucky the cylinder and piston looks ok, besides the connecting rod, the valves/stem seals might also be damaged.

  • @HomelabExtreme
    @HomelabExtreme 3 роки тому +7

    This is exactly what happens if you run a drained engine.
    I have experimented with this on briggs engines, and if they run out of oil slowly (never topped up) the rod will heat up, and snap eventually.
    But if it's fully drained, the rod will bind so hard and fast that the friction will kill the engine before the rod snaps.
    I don't know why you would do it, but to me it looks like the engine had been drained (for storage/transport maybe?) and it was started, died, and then oil was added in an attempt to save it to no avail.
    It takes very little lubrication to prevent the piston from binding to the cylinder, so usually you won't see piston damage when they run out of oil like you would if it overheated.

  • @kevincampbell9619
    @kevincampbell9619 3 роки тому

    Thanks!

    • @jcondon1
      @jcondon1  3 роки тому

      Thanks Kevin for the super thanks!

  • @somerandomguy3868
    @somerandomguy3868 3 роки тому

    Excellent video James, looking forward to the solution for this unit

  • @tedheierman1181
    @tedheierman1181 3 роки тому +1

    I think you could clean up the crank journal then replace the rod.

  • @jmccullough7755
    @jmccullough7755 3 роки тому +1

    I had a riding mower with the same problem. Someone changed the oil and forgot to refill the oil before cranking it. I changed the connecting rod and that took care of the problem.

  • @Melicoy
    @Melicoy 3 роки тому +2

    In case no one said THANKs for telling us the PRICE !!!!!

  • @YukonHawk1
    @YukonHawk1 3 роки тому

    Well.... hopefully you'll find the specs you need.....if not....you have some good parts for other gennys.👍👍

  • @isettech
    @isettech 2 роки тому

    Thumbs up for teaching me to use water.

  • @philn1601
    @philn1601 5 місяців тому

    I have learned how to fix automobiles but now I am learning about generator as well. After the hurricane Beryl I have to keep my Chinese generator running for 7 days straight.

  • @ron827
    @ron827 3 роки тому

    Electric overhead hoist, very handy!
    TEASER!

  • @butler386
    @butler386 3 роки тому

    Wow. That was one of the most unusual stuck pistons I have seen especially with no real evidence of serious damage to crank or rod. This is one that you may not be able to recoup your money from. That would be a bummer. You may have another engine that you can bolt up to the generator and be done with it. Looking forward to next video..

  • @algonzalez8798
    @algonzalez8798 3 роки тому

    Motor has been run low on oil......rod bore can be honed and crankshaft can be polished to get the proper clearance needed. I would also replace those rings and give the cylinder a quick hone with a three stone hone.

  • @rayshutsa6690
    @rayshutsa6690 2 роки тому

    Thank you for another great tare down video. If it is the connecting rod ot might be worth fixing.

  • @treborupp
    @treborupp 3 роки тому +1

    Condon Cliff Hanger....

  • @harveypaxton1232
    @harveypaxton1232 2 роки тому

    Hello James. I enjoy your videos very much.I was wondering why you don't have a hydraulic lift table or cart to place things at a better working height? You are alway working on the floor. Keep up the good work!

  • @markae0
    @markae0 3 роки тому

    Great tear-down video! Loved the disassemble. I'm half way so far.

  • @ScottyStock
    @ScottyStock 3 роки тому +1

    so how does the crank get bigger or the rod smaller? or are we thinking one of them has gone all oval?

    • @jcondon1
      @jcondon1  3 роки тому +1

      Thinking the rod is oval or maybe some foreign material got embedded between the crank and rod?

  • @deepwinter77
    @deepwinter77 3 роки тому +1

    Would this type of Generator be able to run a small to medium welder. 230v 16amp is what the welder requires.
    I'm Europe Ireland so our supply is 230v anyway.
    But I'm unsure if these would be ok for that type of load.
    There's a big jump in price from this type of welder to a more well known Brand.
    Thanks.

    • @jcondon1
      @jcondon1  3 роки тому +1

      It depends on the type of welder. This generator will max out at about 30 amps 240 volts. Would think a new inverter welder would be fine since this is brushed with an AVR the power is cleaner and better suited for the inverter welder electronics. If an old welder with large transformers, not sure. The surge will be 2 or 3 times the 16 amps. Might be tough for an engine this size.

    • @deepwinter77
      @deepwinter77 3 роки тому

      @@jcondon1 it's an inverter welder I just wasn't sure if there able to run that kinda of load, thats good news.
      Ideally I'd like a diesel petrol is very expensive in Ireland, the petrol generators are cheaper but the diesels save you a fair amount on fuel.
      I have a look out for a used welder generator, Mosa preferably they're a well known Brand over here made in Europe known for engine welders and generators.

  • @pete70091
    @pete70091 3 роки тому

    Someone's been watching Taryl Fixes All for that flywheel removal technique. Works every time.

  • @rogerandlyndabeall3840
    @rogerandlyndabeall3840 3 роки тому +1

    They call Chin35e made tools " single use" for a reason! Buy a Ch1n353 generator, use it 2 hours, chuck it in the bin

  • @chriscarlson3557
    @chriscarlson3557 Рік тому

    Water Trick -- IMPRESSIVE!!

  • @leodanryan966
    @leodanryan966 3 роки тому

    Generator Guru? Uhh..that would be you sir. Thanks for the video.

  • @larrykelly2838
    @larrykelly2838 3 роки тому

    Can't wait to see the results.

  • @craigtimmons3468
    @craigtimmons3468 3 роки тому +1

    A new rod, emery cloth to clean the crank up, ball hone the cylinder, new rings and gaskets and a rotator cup for the valve and she should be as good as used.

    • @JohnSmith-yv6eq
      @JohnSmith-yv6eq 3 роки тому

      May have to skim turn the outside of the piston for more clearance as well...

  • @markroth9827
    @markroth9827 3 роки тому +1

    Thank you for your video.

  • @larrysmith3374
    @larrysmith3374 3 роки тому +4

    Could the interference be something that just got cooked onto one or both surfaces. It almost looks like that in the video. Maybe try checking the clearances between the two surfaces? Also, maybe try aggressively cleaning to see if the rogue material can be cleaned off. As you mentioned, maybe it’s something that was ingested through the holes in that air filter and got cooking onto the connecting rod or crankshaft. Seems like that would be worth a try.

    • @jcondon1
      @jcondon1  3 роки тому +4

      Good point. I did not think of that.

    • @erik_dk842
      @erik_dk842 3 роки тому +1

      @@jcondon1 You can use muriatic acid to etch away the aluminum from the rod on the crankshaft

    • @williamvaughan1218
      @williamvaughan1218 3 роки тому

      @@erik_dk842 sodium hydroxide works also.

    • @erik_dk842
      @erik_dk842 3 роки тому

      @@williamvaughan1218 I think the muriatic is faster, but it sure smells bad. Kind of good, because the sodium hydroxide doesn't smell, but eats skin just as good as the acid.

  • @DeadKoby
    @DeadKoby 3 роки тому

    How strange. One would think that if there was extreme wear from rod to crank that there would be shavings and a loose fit. Learn something new every day.

  • @jonminer9891
    @jonminer9891 3 роки тому +1

    Hi, James. So, it ran out of oil and damaged the crank bearing. They put in the wrong bearing. Now it is too tight to turn. Just a guess. Thanks for sharing! Stay Healthy!

    • @JohnSmith-yv6eq
      @JohnSmith-yv6eq 3 роки тому

      There is no seperate big end bearing on the rod.....

  • @sofjanmustopoh7232
    @sofjanmustopoh7232 3 роки тому

    I would be able to take it apart
    But it would in pieces that I cannot put back together.
    Kudos for your great tips.n work
    Maybe the generator part could be put on other engine

  • @knockywigglesworth1909
    @knockywigglesworth1909 3 роки тому +2

    Take the rod to a good machine shop, ask if they can polish crank & hone rod big end...

  • @AntonioClaudioMichael
    @AntonioClaudioMichael 3 роки тому +2

    Hmm something wrong with the piston and the bore not the crankshaft 🤔🤔

  • @hpdepasse5997
    @hpdepasse5997 3 роки тому +1

    a crankshaft pin which inflates is unexpected.
    there are signs of wear on the piston so this engine did not leave the factory with a connecting rod that was too tight.
    I think this engine was reassembled with parts that do not match between them. probably a new rod.
    if the piston and piston ring clearance are good, polishing the crankshaft crank pin and connecting rod to achieve proper clearance should suffice.
    do you know Plastic-Gauge ?
    At the end of the video, the carburetor side flame could indicate improper ignition and/or camshaft timing.

    • @jcondon1
      @jcondon1  3 роки тому +2

      I will use plasti-gauge next week. I thought timing at first, but there is an issue with the rebuilt engine.

  • @dimastonny1238
    @dimastonny1238 3 роки тому

    saya suka sekali vidio kamu jemes condon👍👍 trimakasih berbagi pengalaman👍🙏😊👨‍🔧👨‍🔧👨‍🔧
    salam kenal dari surabaya jawa timur indonesia🇮🇩🇮🇩

  • @AZVIDS
    @AZVIDS 3 роки тому

    Very cool. What a tease👍