Joseph Krug
Joseph Krug
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Ipad stand from wood scraps
So I have not yet gotten motivated since it has been super hot outside (ie 25F higher than normal for our area) to work on the new box lids, but I havd been reading at my computer desk on my ipad. And the way I have been propping it up has been a small box with a video game controller...but that is too light at times, and sometimes falls over, which causes the corner of said box to poke the 4k monitor....which is not ideal, as eventually it will I am sure screw up the monitor...so I decided to try and make a quick ipad stand out of wood scraps. And it looks to work fine, with only one handsaw cut and a quick notch, then some screws to hold it together.
Переглядів: 76

Відео

New recipe box lid comparison/choices
Переглядів 4521 день тому
So back in 2022, I made a fancy recipe box for my sister: ua-cam.com/video/bwN-TQObR7M/v-deo.html And when I asked her what other projects she thought I should try, since I now have an etsy store, she suggested a few more recipe boxes. So those are in progress...I have the sides sorted out, and now need to figure out what sort of combinations of different wood scraps to use for the stripes. So ...
Non-project video - wrists and shoulders
Переглядів 2121 день тому
Since this is not a project video, I wasn't sure if anyone would be interested, but my wife said I might be surprised. So here it is, this video covers what works for me to keep my wrists happy again when the bones get out of place, and what exercise/range of motion thing that I have found works for me when my muscles get really tight where my spine meets the shoulders. The range of motion thin...
New hammer for the replaceable heads
Переглядів 178Місяць тому
Since I figured out that the original stainless 'head' where the replaceable heads attach was defective wrt the metal head threads, I was insane and decided to make a stainless steel replacement head and new handle...to work with the brass and aluminum heads. Well.....it was a success, even though I now know why people say working with stainless steel is a pain...that is due to it being a pain ...
New lathe chuck key
Переглядів 541Місяць тому
I noticed as I was working on the new aluminum hammer end that the home made chuck key that came with the lathe...and had an original 'twist' to the end...was twisting even more. So I decided to order a new 1/4" chuck key on ebay...for the 1/4" chuck...but in this video found out (like a comment on the ebay listing) that I did need to grind some off so it would fit...as a 1/4 peg does not fit i...
Replacement hammer head part 2
Переглядів 32Місяць тому
Well...after using the die that got here, it is a difference size than any of my die wrenches...so needed to use a 17mm wrench on it instead which is not ideal. Then by doing an undercut at the back of the threads, it does mostly fit into the head center piece on one side but still does not seat completely. The other side it is crooked...and so due to the issues it still has, it still will not ...
Replaceable hammer head - make new end part 1
Переглядів 104Місяць тому
So as I ran into in my last video on making the pulley key way for the cutter grinder, the brass and aluminum heads for the replaceable head hammer...suck. And by suck I mean the fitment is such that it only holds on the threads vs having a clean seat of the replaceable hammer head against the head body. That is a recipe for disaster as I found out, as it stripped the brass threads right off th...
Deckel SO Cutter Grinder - new belt and pulley works
Переглядів 60Місяць тому
So I was able to get some 4mm Round belt on amazon: "Round Belt 4mm OD 13Ft High-Performance Urethane Belting Green" and then was able to melt that together, clean it up, and after doing a quick 'material removal' for the guard, was able to get everything installed and working. Also put a piece of cork board under the motor to try and reduce vibration..not sure if it helped or was really needed...
Terratek Grinder new wheel - works
Переглядів 35Місяць тому
So after more research and not knowing how much I will use this grinder, I decided to spend enough to get a good half inch arbor size fine wheel vs a more expensive CBN wheel to start. If I use the grinder a lot and find out I need the functionality of a CBN, then it may be worth upgrading, but for now, the goal is to just get it up and working like new and see how well it works. So far, looks ...
Deckel SO Cutter Grinder replacement belt issues
Переглядів 382 місяці тому
So now that the new motor and first test pulley are installed, next is to figure out the new belt sizing. Of course it cant be that simple, as due to the new motor being larger, the pulley location shifted, and that causes the new belt location to impact the one unused attachment point on the shroud that was used to attach the built in dust collector that I do not have. So I have to decide if i...
Terratek 6" bench grinder TBG62LA - what size/grit CBN wheels would you recommend?
Переглядів 842 місяці тому
So I got a free 6" bench grinder from a friend from work who was not using it (Thanks Tom!). It is a Terratek TBG62LA grinder which uses half inch arbors that currently has a fine grit wheel (6x3/4x1 inch center hole) and coarse wheel installed (6x3/4 with half inch center hole). The fine wheel has a set of plastic inserts to act as a spacer from the 1 inch hole to the half inch arbor. Unfortun...
Deckel SO Cutter Grinder motor mounts for new 220v single phase motor
Переглядів 1192 місяці тому
Now that the first test pulley is done (still may need to make another one if it runs into problems later, who knows), I am able to work to make new motor mount adapter pieces to get my new 220v single phase motor to attach to the unit instead of the original three phase motor. I used 1/4-20 machine screws with the slanted heads for the attachments between the adapter plates, the original plate...
Cutter Grinder Pulley part 3 - worked!
Переглядів 1222 місяці тому
I finally got motivated to try and finish the pulley today. Initially I tried to use the boring bar setup that came with the little machine shop kit that I got for my lathe, but something in the setup was not right, as it was bending instead of cutting. Maybe I should have tried the shorter bars first, but I figured the thickest longest bar was what I needed to get through the pulley, but it de...
Time to replace a 1997 era water heater
Переглядів 1,1 тис.2 місяці тому
This video is not that exciting, it just documents that we finally had to replace the 1997 era water heater that our condo came with back in 2004 as it is finally spewing out rusty water with some corroded bits. Now we have a new one that will likely 'not' work as long as the old one, but hopefully will do well for its entire life. Another appliance is gone from an era where things were built t...
Hathor rattle stand height extension
Переглядів 872 місяці тому
So my wife liked the stand I made for her Hathor musical rattle, but she had originally thought she wanted it taller...and after using it for a week, still wants it taller. That way it does not tilt back and bump into the mirror behind the bed. So I took the off cut from the original board, and made a height extension. She likes it a lot, so that is a success.
Drill press cabinet fix for my Rockwell Delta 15-665
Переглядів 1252 місяці тому
Drill press cabinet fix for my Rockwell Delta 15-665
Cutter Grinder pulley lathe project part 2
Переглядів 2652 місяці тому
Cutter Grinder pulley lathe project part 2
Craftsman 6-18 lathe tail stock issues
Переглядів 4142 місяці тому
Craftsman 6-18 lathe tail stock issues
Cutter Grinder pulley lathe project part 1
Переглядів 1072 місяці тому
Cutter Grinder pulley lathe project part 1
Box fan amperage test
Переглядів 742 місяці тому
Box fan amperage test
Box fan bearing replacement
Переглядів 7852 місяці тому
Box fan bearing replacement
Stand for Egyption style musical rattle
Переглядів 1602 місяці тому
Stand for Egyption style musical rattle
Reamers set 1/16" to 1/2"
Переглядів 483 місяці тому
Reamers set 1/16" to 1/2"
Recipe boxes preview
Переглядів 683 місяці тому
Recipe boxes preview
New Samsung DU7200 board failure in less than one month
Переглядів 5993 місяці тому
New Samsung DU7200 board failure in less than one month
Lathe cart drawers
Переглядів 1574 місяці тому
Lathe cart drawers
Craftsman air compressor after cooler project is done
Переглядів 774 місяці тому
Craftsman air compressor after cooler project is done
Craftsman 919.167280 air compressor after cooler
Переглядів 3014 місяці тому
Craftsman 919.167280 air compressor after cooler
Bad fittings from SDTC Tech, ie undersized and do not work reliably
Переглядів 394 місяці тому
Bad fittings from SDTC Tech, ie undersized and do not work reliably
First Lathe project - fix bad air fitting
Переглядів 404 місяці тому
First Lathe project - fix bad air fitting

КОМЕНТАРІ

  • @silverbullet7434
    @silverbullet7434 День тому

    Cast iron it should be brazed first it needs a small hole drilled at the cracked. Ends. Thick washer should help tee slot .its a nice lathe get some books one how to run a lathe by south bend ??

    • @josephkrug8579
      @josephkrug8579 День тому

      Thanks, yeah rather than fix that one (though I kept the old part), I bought a new one freshly manufactured out of steel off of ebay. I did download the south bend books off the internet...need to read through them and find more lathe projects to make. Since that video I made a replacement pully and a hammer body/end in future videos. So far, for what I need (minimal lathe needs) this lathe has done great.

  • @Dawna-y2c
    @Dawna-y2c День тому

    Yeah I hope that takes out all the slack

    • @josephkrug8579
      @josephkrug8579 День тому

      @@Dawna-y2c It has been a lot better since then, so it definitely helped.

  • @mcds54
    @mcds54 3 дні тому

    Just got a 2024 Samsung qn90d (98-inch). The retail store where I bought it (not Samsung) eventually sent out their own techs to replace the PCB and adjoining straps due to memory issues causing service menu errors. Works great now. The tech said that he's had to do this 4 times recently, even with other brands. So much for QC.....🙄

    • @josephkrug8579
      @josephkrug8579 3 дні тому

      At least it was fixable during the warranty....too bad the warranty periods are so short anymore...but with hardware issues like this, that is not a surprise. Glad you got yours fixed too....so far the fix has worked great for my neighbor...no issues yet since this got fixed.

  • @davidparker3346
    @davidparker3346 9 днів тому

    You can put it in my garage.

    • @josephkrug8579
      @josephkrug8579 9 днів тому

      So far I have made two successful projects on it. :) The pulley went the best, the hammer....made me realize why people hate working with stainless steel....it still worked tho and so counts as a successful project. There are wear issues that make it a slight challenge to use tho, ie the biggest is the backlash in the various wheels for moving the carriage etc. Still worth it I think.

    • @davidparker3346
      @davidparker3346 9 днів тому

      @@josephkrug8579 I have one of these that I would like to do cosmetic restoration on. It works fine it just needs to be cleaned up and repainted.

  • @ebwalk03
    @ebwalk03 14 днів тому

    Thanks! Could they have made it any more difficult?

    • @josephkrug8579
      @josephkrug8579 14 днів тому

      Yep, they could have hidden it so you could not look down in to see how the mechanism works. :) Luckily they made it as 'easy' as they did so we have a chance to get it to work right ourselves. Just think of how annoying it would be to have to make an appt with some paid service to have them come change the sandpaper...bleh. This way we can at least do it ourselves. :)

  • @mrk1075
    @mrk1075 16 днів тому

    You can get a defective tv from any brand tv. We bought five Samsung TVs since 2018 and there all still working! 🙂

    • @josephkrug8579
      @josephkrug8579 16 днів тому

      Well the good news is it is still working so far for my neighbor since the fix. Hopefully it will stay that way.

  • @josephkrug8579
    @josephkrug8579 21 день тому

    So far for the non youtube comments, I have had people like option 2, 3, 4, and one person said if I moved the red swirl pieced from 5 into 1 instead of the walnut or oak, they would like that one better. So far though option 4 is in the lead.

  • @josephkrug8579
    @josephkrug8579 22 дні тому

    It is always a challenge when building things from scraps taken from repurposed furniture, etc. What kind of stripes do you like?

  • @RustyInventions-wz6ir
    @RustyInventions-wz6ir 26 днів тому

    Very nice work sir. That looks like a handy hammer

    • @josephkrug8579
      @josephkrug8579 26 днів тому

      Thanks, It was a lot of 'first time' attempts...especially with the stainless steel, so I am happy it turned out as a usable hammer. :) It is especially nice that I can re-use the brass head the original hammer screwed up the threads on.

  • @benjaminarmstrong5550
    @benjaminarmstrong5550 29 днів тому

    i have a craftsman quarter inch drive rachet with a extension that lives on my lathe bench saves a bunch of time. Somtimes ill even sin and put a quarter inch driver in the drill and really speed things up.

    • @josephkrug8579
      @josephkrug8579 29 днів тому

      Nice, I dont use it enough yet to warrant needing a drill for it, but that is a good reminder that it could work :)

  • @gregbarber8659
    @gregbarber8659 29 днів тому

    I was fighting with mine for over an hour just because I didn’t know where that tail was supposed to go. Thank you

  • @josephkrug8579
    @josephkrug8579 Місяць тому

    I am glad this ended up working along with the original metal heads in the new hammer body I made in an upcoming video. That gives me the flexibility and confidence that if i need another new head end like this that I can make one.

  • @StanleyRestall
    @StanleyRestall Місяць тому

    I have the same problem BUT only on one of the chuck square drives. It fits one hole fine but not the other two 🙂

    • @josephkrug8579
      @josephkrug8579 Місяць тому

      @@StanleyRestall Well if u decide to grind on it, make sure your tables in front of the grindstones are square and measure often vs doing what I did. 🙂 I took a bit too much off and the result was not square.

    • @josephkrug8579
      @josephkrug8579 Місяць тому

      And maybe carefully measure the hole it does not fit in...and make sure there is no debris in there. It could be it is slightly off in size in one dimension vs the other.

  • @josephkrug8579
    @josephkrug8579 Місяць тому

    I definitely needed the new chuck key to work with the stainless hammer head lathe project that I also worked on and finished this weekend.

  • @rtel123
    @rtel123 Місяць тому

    All the new water heaters still line with glass, as far as I can determine. Dunno why they told you it is not. Cheap to do, so why stop? Also, draining a tank is easy: just open a hot faucet somewhere and the air will rush in. Also strange that the TPR valve has so many elbows for the discharge. Just needs to go sideways and out.

    • @josephkrug8579
      @josephkrug8579 Місяць тому

      I eventually got it sorted and the hot water is way faster to heat for the new one. So this was a definite win.

  • @RustyInventions-wz6ir
    @RustyInventions-wz6ir Місяць тому

    Very nice work. I think your fix is better than before.

    • @josephkrug8579
      @josephkrug8579 Місяць тому

      Thanks :) I will know for sure when the m8 1.25 die gets here and I see if I can properly get threads on that new longer section. At least I have lots of aluminum bar to try again if it does not work, and it really did not take long to make that new piece. If this works I may buy a chunk of 1.125" diameter (1 1/8 x at least 2 inches long, probably 6 inches ) brass off ebay and try and make a similar brass replacement head.

  • @eleanorkrug8694
    @eleanorkrug8694 Місяць тому

    Good job

    • @josephkrug8579
      @josephkrug8579 Місяць тому

      Now we just have to see if I can find projects that will need this or not. :) But at least it runs with the new motor.

  • @josephkrug8579
    @josephkrug8579 2 місяці тому

    I decided to order some of the do it yourself round belt off of amazon...we shall see how that goes once it gets here.

  • @dennisemme2456
    @dennisemme2456 2 місяці тому

    Try tightening the two Allen's on the compound rest. They lock it to what ever angle you want it to be at.

    • @josephkrug8579
      @josephkrug8579 2 місяці тому

      Thanks, I think I since solved that issue since the video came out. :) Good to know people are helpful though, I do appreciate the information.

    • @dennisemme2456
      @dennisemme2456 Місяць тому

      @@josephkrug8579 you could also set the compound to be parallel twitch the bed rails. Would then allow fine feed when facing.

  • @tdok6487
    @tdok6487 2 місяці тому

    Great video. I just picked a set up today after watching this last night. I have one side adjusted, not to do the other side. I want to find a safe way to push the buttons to drop the table, the way they designed it you can cut the tip of your fingers.

    • @josephkrug8579
      @josephkrug8579 2 місяці тому

      Yeah, the way those buttons work you have to be really careful with the table weight to not pinch/damage your fingers. One solution if you have space (I do not) is to leave them up all the time. Or, only use them for longer pieces where you need them, both would reduce the number of times you have to raise/lower them. Luckily I normally run somewhat shorter pieces (< 16 inches) so most times I do not use the table, but the times I do I definitely take extra care when lowering them due to the danger to the fingers. If I come up with a good idea to make that safer, I will make another video on it. But for now, just be extra cautious when doing that and never do it 'in a hurry'...or you may have issues as you realized.

    • @tdok6487
      @tdok6487 2 місяці тому

      @@josephkrug8579 I worked in tool and die for a few years. I was trying to think of a way to add a piece over the button to push it in. The ironic part is the sticker next to the button saying not to use your fingers to push it. Ok, what other options do they suggest? lol

  • @josephkrug8579
    @josephkrug8579 2 місяці тому

    Or do people just recommend the normal non-cbn wheels for a 6 inch grinder?

  • @josephkrug8579
    @josephkrug8579 2 місяці тому

    Hopefully someone who watches this will know if a 6 inch grinder that comes with 6x3/4 thick x 1/2 arbor grinding wheels can also use the 6x1 x 1/2 arbor CBN wheels. And if so, if they have any recommendations on the best grits to use if you already have another sharpening system such as the worksharp ( which I do ). Or do people just recommend normal grinding wheels and not cbn? Those are definitely cheaper.

  • @firstnationsindian8062
    @firstnationsindian8062 2 місяці тому

    The moral of the story is , stop buy chinesium.

    • @josephkrug8579
      @josephkrug8579 2 місяці тому

      Unfortunately with the flood of that in there, It is sometimes hard to find anything else on amazon.

  • @Cru-JohnNicholson
    @Cru-JohnNicholson 2 місяці тому

    Whoa! So glad I saw your video. I like to fix things and usually I can fix lots of broken items. I was thinking, "How hard can it be to replace a little pad somewhere?" Uh....no, after seeing this, the correct option is pretty obvious - buy a new printer. I'll probably try to take the old one apart just to scavenge for interesting parts. Thank you!

    • @josephkrug8579
      @josephkrug8579 2 місяці тому

      Well, it all depends on what your error is due to....it could be just the heads which is not as bad a fix, but if it is what i found, yeah, new printer for sure. The issue was I think caused by the lady who owned it using office max cartridges which had at least once gone bad and leaked a lot. There are a lot of nice stainless steel shafts that you can harvest from these printers, like I did with this one. :) Good luck.

  • @robertnirenberg4556
    @robertnirenberg4556 2 місяці тому

    I have one of these lathes, old but fun. The factory taper for the tailstock should be a stubby MT-0. The only tooling i saw there that looked like a zero is that smallest chuck. I suspect that the previous owner, or one of them at least, modified it to take MT-1 tooling as that's more common. But im just guessing from what you showed in this video. Good luck and keep having fun with it!

    • @josephkrug8579
      @josephkrug8579 2 місяці тому

      Thanks :) When I looked on the Little Machine shop website while trying to get the quick change tool post etc ( littlemachineshop.com/products/product_view.php?ProductID=3593&category=2122081985 ) , they said that the mt-1 was more common but the mt-0 was a possibility. measuring it I saw it was the mt-1 size which I got. Yeah it could be that one smaller one is for the mt-0. Maybe the conversion that a previous owner did is why the tail stock gauge is not right too. Maybe i will be able to figure it out when I take that apart at some point to investigate why the handle/etc is bent and wobbles. Until then I will try and have fun with it. :) Without major lathe projects it should be a good size to help me learn what to do, etc. At least it has been able to do that so far. :)

    • @M1KEMEX
      @M1KEMEX Місяць тому

      @@josephkrug8579 Wrong. The 618 uses MT1. I also have one.

  • @KennyCrawford426
    @KennyCrawford426 2 місяці тому

    When you retract the tailstock, it will eject. That is not a defect but how it is designed. The drill chuck has a full tang taper. You could reduce this by grinding off the flat tangs on the back. Be careful. If you go too far, it will not eject anymore. The limited travel on the tailstock is because it is a very small lathe. You can buy reduced-length or "stub" length MT tapers for small machines. I am not great at videos but I have a couple smaller lathes and some tooling, if I can figure out how to post a video (its been a while) I could show you what I am talking about. That is pretty nice looking old lathe you have there.

    • @josephkrug8579
      @josephkrug8579 2 місяці тому

      Thanks, when I saw it on either craigslist or facebook marketplace, I had to check it out as it had so many accessories and was a mile away. :) Yeah I now realize better that when it gets to the end it kicks out the tool, and that is good and better than it being stuck permanently. It is still possible that someone who owned it before me messed with something in the tailstock (still have not opened it to check yet) as the handle is bend and wobbles...And the other issue may indeed be all of the tapers I have are too long for this lathe. I would rather not cut the ends off things like tapers as that ruins the flexibility of the tool to use in the future for a different lathe...even tho I do not yet have another one I like to try and retain all the future options where I can. The one really short taper shaft that I had shown for the smallest drill chuck, doesn't even fit this lathe as I found out...when I tried it last night to see if the shorter one would work. I will get it figured out eventually. :) Especially with all the good comments people keep leaving on the various videos.

  • @mans4104
    @mans4104 2 місяці тому

    You advance the tail sock further in and continue drilling. Lets say 3/4" at a time.

    • @josephkrug8579
      @josephkrug8579 2 місяці тому

      Thanks, I did try that a bit, but it didnt help remove the chips, ie they kept getting clogged then I had to stop, pull it back out, clean it off and try again. One other suggestion I saw was that my bits and tapers may be too long for this lathe...ie those end tabs may not be needed, or were for other lathes not mine, so they said I could always trim those off to get some of the extension back as well. I would prefer not to do that but at least I know it is an option.

  • @RustyInventions-wz6ir
    @RustyInventions-wz6ir 2 місяці тому

    Very nice work sir.

    • @josephkrug8579
      @josephkrug8579 2 місяці тому

      Thanks, hopefully the rest of it goes well, otherwise it will be time to start on the second aluminum chunk and try again. :)

  • @RustyInventions-wz6ir
    @RustyInventions-wz6ir 2 місяці тому

    Very nice work sir

    • @josephkrug8579
      @josephkrug8579 2 місяці тому

      Thanks, I am glad I did not have to cut everything shorter to fix...widening the holes in the back and then fighting repeatedly to wiggle it into place was less work for sure.

    • @RustyInventions-wz6ir
      @RustyInventions-wz6ir 2 місяці тому

      @@josephkrug8579 He he. Not everything works always to plan

  • @fredjones1238
    @fredjones1238 2 місяці тому

    whats the biggest diameter you can put in it

    • @josephkrug8579
      @josephkrug8579 2 місяці тому

      @@fredjones1238 The lathe will do up to 6 inches in diameter and 18 inches long. But even for aluminum you have to take tiny cuts, so keep that in mind.

    • @fredjones1238
      @fredjones1238 2 місяці тому

      thank you

  • @VanWinger
    @VanWinger 2 місяці тому

    You can lube the bearings in place on some motors using SUPCO zoom spout oil

    • @josephkrug8579
      @josephkrug8579 2 місяці тому

      Thanks, I heard from other people that 20 wt non detergent oil can also work. It is good to know the options. I know that you should NOT use the 3-1 oil from some people, and others said it may work ok, so it is good to know the various options. :)

  • @sccpsteve
    @sccpsteve 2 місяці тому

    The ammeter you used is only accurate to 0.4 increments. Also you can probably only find the weather shield on a popular webstore. The plastic parts (i.e. grilles, feet, blades, handle, knob) are easily available on Lasko's "Encompass" webstore. If the motor in the new box fan is NOT "square" then keep it, the bushing bearing parts are the same. All they need is oil to keep running smoothly.

    • @josephkrug8579
      @josephkrug8579 2 місяці тому

      Yeah I forgot I had one of those kill a watt outlet things, and those would have been more accurate. At least the fan which I replaced the bearing on looks to have similar usage though as the near identical one which has the original bearings. Thanks for the pointer to their store. Similar to the existing fan, the new one has a square motor block....and the new one is the weather shield motor...but just not the fans with the round pattern in the grill. So I will have to decide if I want to keep it or not.

  • @brianroberts4349
    @brianroberts4349 2 місяці тому

    The shaft is a standard 3/8 diameter. The original bushings will last forever if oiled...the felts need to be oiled well.

    • @josephkrug8579
      @josephkrug8579 2 місяці тому

      Where were you and your super useful comments when I was working on trying to figure this out. :) So yeah the 9.5mm is 3/8 inches ID...and the 28.5mm is 1 1/8 inches OD....and those look to be more common and easily found. ie a quick amazon search showed this one which may be a bit too thick, but still is similar sizing: 1614-2RS 3/8“ x 1-1/8” x 3/8" (ID X OD X Width) That would take more measuring to figure out the width as i do not remember offhand the thickness needed given the spacing...and did not write that down, For some reason since these were 'modern' fans I figured they would be all metric and so looked that route. Should have done the sae sizes too. Thanks. Once the bearing dries out and cooks the shaft, ie leaves a burn/whatever mark on it, that would indicate the oil dried out. In that case if you wanted to go that route the shaft and collar would need cleaned thoroughly and then the oil re-added. Do you know by chance what kind of oil should be used? That would be another way to go for fixing these fans.

    • @brianroberts4349
      @brianroberts4349 2 місяці тому

      @@josephkrug8579 I have taken apart at least 20 various fans/motors with those type of bushings. There has been not one single case where cleaning up the axle/shaft and the interior of the bushing of any dried oil and then oiling well that the motor/fan has not worked fine. They aren't high tolerance bushings. Just a light weight household 10-15 wt oil. 3-in-one is fine....but...be aware...they do make a heavier 3-in-one that may be too thick.

    • @josephkrug8579
      @josephkrug8579 2 місяці тому

      @@brianroberts4349 Thanks, I heard from others that 20 wt non detergent oil works too. It is good to know the options for sure. As I know lots of other people just throw them out and buy another one, which I would prefer to not do.

  • @Autojurk
    @Autojurk 2 місяці тому

    i recently obtained the same lathe, atlas 618, and my compound had been broken and welded back together in the same spot, but on the other side its not something i would recommend trying to weld, but it can be done with nickel rods and some skill, or brazing, maybe even silver soldering but what i would recommend, is ditch the compound totally and make a riser block to the QCTP, just get a chunk of something decent, and machine the round hole and drill and tap some set screws, or something to that effect keep in mind, your tool holders have some wiggle room up and down to get onto centerline but this is also 2 months after this video and chances are you have come to all these conclusions already hehe

    • @josephkrug8579
      @josephkrug8579 2 місяці тому

      Thanks for the comment. :) Yeah since then I had bought the solid steel replacement, and other than still needing to make a better t block for that out of the piece of metal that the little machine shop included with the kit I got, it works well enough that I am attempting the replacement pulley for my cutter grinder on the lathe. I learned a lot so far with doing that, including that I needed a thicker parting blade as the 1/16" one that came with the kit is too floppy. I also learned that it is best to have one hand on the back and forth and one for the in out wheels when doing work,as the play is enough that things float slightly....and cause extra cutting noise. The thicker cut off blade should get here tomorrow so once I make more progress and either have a working pulley or a failed one that I have to re-do, the video will get posted for that. :)

    • @Autojurk
      @Autojurk 2 місяці тому

      @@josephkrug8579 i totally know what you mean about all hands on deck when cutting, i have a lot of slop in the screws as well, but such is life i suppose. i saw your video on the new steel compound after i made my comment and thats a slick bit of kit for sure, but ouch at the price, i think at some point i'll take a shot at making my own but with t slots down the length rather than just the end, so i can mount other things in there. two suggestion i have for these lathes, one whimsical and one not so much, treadmill motor repower, and an electronic lead screw, the treadmill motor being easy to obtain for sure. oh and for sure the riser block to kick the compound ot the curb til you have to thread or cut a taper

  • @josephkrug8579
    @josephkrug8579 2 місяці тому

    Wife likes it so far, the far right image in the thumbnail is where it ended up once it was all done.

  • @jul371-y5p
    @jul371-y5p 2 місяці тому

    experiencing the same problem, but dremel wouldnt take care of it because thewarranty ended, they told me to buy a new one instead lmao

    • @josephkrug8579
      @josephkrug8579 2 місяці тому

      Yeah I was lucky that it was within the warranty...I guess that shows if you buy a new tool, or anything with a warranty, test it thoroughly right away.

    • @jul371-y5p
      @jul371-y5p 2 місяці тому

      @@josephkrug8579 was working just fine until today that i needed to use a grinding stone instead drill bits, started wobbling non stop pretty ass response to "buy a new one look" just guess they dont make it like the old black ones

    • @OlDirtyBandit
      @OlDirtyBandit Місяць тому

      @@josephkrug8579I bought one brand new that did this out of the box. Dremel is ok for being cheap but if you plan to use it daily don’t waste your money

  • @dazzhan9826
    @dazzhan9826 3 місяці тому

    To really stiffen up the bench get some plywood (minimum 1/2 inch thick) and screw it onto the back and sides - same as in house construction. That will significantly reduce twisting and movement of the bench. I managed to pick up a Craftsman 618 lathe from Facebook, that came with a great assortment of accessories, and a homemade wooden bench. Unfortunately I'll have to dismantle the bench, shorten the legs, and rebuild it with better joints and plywood for the back and sides. It has a double layer plywood top, but it's not straight. I'm leaning towards a 1/2 inch steel baseplate for the lathe to mount on, then shimming that base where necessary to match the bench's top.

    • @josephkrug8579
      @josephkrug8579 3 місяці тому

      Yeah, that is why when I built the bench for this, I put so many side to side stiffener pieces in the top section. Same for why I put the multiple layers for the actual top. And I did screw a piece of plywood to the back after installing the drawers, but i don't know if I included that in a video as screwing a piece of plywood to the back of a cart is not that interesting in itself. :) Given the results of the precision level that i did in a different video, I think the top of this one should be fairly solid and not twisting much. the bigger issue is the garage floor slope and angle...sometimes when I move the cart not all the wheels touch which also means the cart is stiff as otherwise it would conform to the floor when I move it around. Good luck with your cart re-do as well. :)

  • @RalfyCustoms
    @RalfyCustoms 3 місяці тому

    Lovely old machine, I have a 10F, without all those accessories mind you, the 45 looking tool, is most likely a 60º thread turning tool btw

    • @josephkrug8579
      @josephkrug8579 3 місяці тому

      Thanks :) As I mentioned in the video, when I saw it was a mile away with all those accessories....I had to go get it. My next lathe project will be the replacement pulley for the cutter grinder I got that will fit the new 220v vs 3 phase motor that I got for it.

  • @markh351
    @markh351 3 місяці тому

    I've heard that Samsung's quality control has gone downhill starting a couple of years ago. I bought my Samsung TV in 2018 and noticed some significant flashlighting at the bottom of the screen in the corners and in the middle. I gave them a phone call, and they replaced the panel within two weeks and it's been good ever since. Still running it now. That said, my next TV won't be a Samsung after what I've heard in recent times, plus the lack of Dolby Vision and DTS passthrough on their sets.

    • @josephkrug8579
      @josephkrug8579 3 місяці тому

      Yeah that is making me worry about our 10+ yr old LG tv as well...it snuck in before the whole smart tv mess....and so I hope it lasts for a while, as the smart tv mess is not something that is fun to deal with.

  • @TonyLiveTV
    @TonyLiveTV 3 місяці тому

    I was strolling along and came across your video. I see you are strapped for space, but I think there is a solution. On the compressor side you currently are going directly to your hose reel I believe. What I might do instead is remove the regulator from the tank and attach a whip hose directly from the tank to the regulator which you would install on the wall. From there you can place a small manifold and attach a filter/water/oil separator. From there you can place your desiccant drier all on the wall behind your compressor. On the manifold side I have a valve so I can direct air to the desiccant when I need dry air or I can bypass the drier when I don’t. This saves on replacing desiccant. You can also reactivate the desiccant in your oven. Cheers 🎉

    • @josephkrug8579
      @josephkrug8579 3 місяці тому

      Thanks, but I already solved this in a future video where I added an after cooler setup instead of desiccant. My problem is that I cant add things to the wall, even with things as small as I have it...as I have to be able to have the flexibility to also roll the compressor out to the parking lot if needed for emergency tire fill ups. That is infrequent enough, and not knowing where in the condo lot we will end up being when needing air, so it has to be mobile vs just a long hose. Also, I do not have space for a second movable standalone portable air tank, so I had to keep everything onboard the compressor setup. The after cooler setup I made definitely works...I have filled the tank from empty 3 times now and zero water made it into the tank. :)

  • @josephkrug8579
    @josephkrug8579 4 місяці тому

    I did the second empty to full fill today, and zero water ended up in the tank when I checked it later with the bottom drain. So far loving this change.

  • @RustyInventions-wz6ir
    @RustyInventions-wz6ir 4 місяці тому

    Very nice work sir

    • @josephkrug8579
      @josephkrug8579 4 місяці тому

      Because I cut the end off that one piece and was tired of waiting for 'bad fitting' amazon parts I went to home depot, bought a 1/4 npt pack of husky fittings and used that to finish the compressor project...ie couldnt return it since I hacked the end off in the lathe (which didnt solve the issue) so may as well make it work anyway. I still do NOT recommend those fittings even if I managed to get it to work eventually buy buying extra parts to use to get it adapted to finally work.

    • @RustyInventions-wz6ir
      @RustyInventions-wz6ir 4 місяці тому

      @@josephkrug8579 I have a compressor that is fairly new, but after the motor packed up I decided to change the lot, just kept the tank. That fittings was a headache to match. He he.

  • @crazysteve2112
    @crazysteve2112 4 місяці тому

    I am dumber by watching this... You should have spent the money buying a REAL compressor instead of that oil-less POS Crapsman compressor

    • @josephkrug8579
      @josephkrug8579 4 місяці тому

      Well I am glad you enjoyed it. :) Did you know that even if you buy one of the more expensive $1000 california air tools air compressors....that you still need an after cooler unless you want to spend closer to $3k to get an after cooler they have built in? Or if you have way more garage space than I do, you could buy one of those refrigerated air coolers, but then it is not self contained, and again takes up space I do not have to put it in. I did price out getting another air compressor, and for all that I use it, I could not justify spending $3k on a new compressor that had an after cooler built in that would fit in the space I have....so..I did the intermediate step and added an after cooler to the one I had. If I need a bigger/better air compressor in the future, this after cooler set of parts will scale up to the new compressor too.

  • @thedevilinthecircuit1414
    @thedevilinthecircuit1414 4 місяці тому

    When engineers write operating instructions without ever having used the item. Quite common.

  • @jerryvan6709
    @jerryvan6709 4 місяці тому

    Why did you use fuel line rated hose and not air hose? Is the fuel hose rated for over 150 PSI?

    • @josephkrug8579
      @josephkrug8579 4 місяці тому

      The hose was listed as 300 psi working pressure....I figured that would be fine for a compressor that only goes at max to 150psi.

  • @josephkrug8579
    @josephkrug8579 4 місяці тому

    Moral of the story is...the air temp coming right out of the compressor is too hot for a rubber line, even a fuel line rated up to 250F...as I measured a temp that hot after i did a full run with the new mcmaster carr hose. So if someone else wants to try this, get your hose length between the compressor outlet and the radiator, and go right to a high temp mcmaster-carr hose...will save you days and days of pain and annoyance.

    • @tjhemrick
      @tjhemrick Місяць тому

      You can get runs of hydraulic line at Tractor supply that are preswedged with ends. They're rated in the thousands of PSI and temps well above any compressor. Like $50-60 for a 4-5 foot piece.

  • @rolliekelly6783
    @rolliekelly6783 4 місяці тому

    Did you ever replace the missing felt oil wick in the bottom of the leaking bearing housing? It soaks oil up from the well in the bottom of the housing and wipes oil on the shaft, this keeps the bearing lubricated yet doesn't allow oil to leak out. To quote Bear Claw: " Seen it right off"!

    • @josephkrug8579
      @josephkrug8579 4 місяці тому

      I did, I put he felt wick back in on both bearings before I put it all together and it is working fairly well so far. ie even used the jointer for a project and the oil did not leak out and the bearings did not get above 'touch' temps. The big key was the grooves to help route the oil back in vs having it all go to the outsides.

  • @emanuele3351
    @emanuele3351 4 місяці тому

    Incredibile la Canon truffa i consumatori

  • @josephkrug8579
    @josephkrug8579 4 місяці тому

    Well as you will see in the final video on the tv...the led replacement worked. However, I screwed up and mis-installed the interior trim piece and screwed up the led panel wiring harness.....and then screwed up the tv....as a replacement panel since those wiring harnesses are built into the panel, costs more than a new tv.

  • @josephkrug8579
    @josephkrug8579 5 місяців тому

    I really need to make time to build the drawers under the lathe so all my tooling/parts have somewhere reliable to go....as I totally forgot that the quick change tool post kit....came with cutting bits: www.amazon.com/Tooling-Package-Atlas-Craftsman-Lathe/dp/B01CF5P94O So I did have cutters to go in there other than the cut off blade. Oh well, less to buy I guess. :) Still need to figure out the milling attachment bits to use though.